Subject: Medical Road Trip
Date: Tuesday, January 08, 2002 9:52 AM
Sunday I
drove the faithful old Suburban to Medford (225 miles) for an appointment with
my cardiologist.. I am trying to get
authorization from him to go ahead with the neck operation I need..
The trip
was a trip. Most of the way it was
blowing about 50 mph gusts with heavy rain..
I felt like I was at sea some of the time..
The
doctor and I aggravated back and forth Monday morning from 9:30 am till 12:30
but I got permission to get the surgery..
The now
desmogged and transmogrified Suburban ran like a dream and when I gassed up in
Medford and figured the milage I was happy to see 19.92 mpg.. And that is with the racing setup on the
vacuum advance can which may be dropping the milage by 2 or 3 mpg..
The trip
home yesterday was more of the same but the Southwest storm winds were up to
over 70mph on the coast so it was interesting bucking those winds in the
torrential rain at night..
But I
got home safely.. Haven’t figured the
milage on the return trip yet..
After
arriving at 6:30 pm and was just getting settled down to make some dinner at
7:30 when the lights went out.. Storm
induced power outage.. Damn..
So I sat
in the dark (and cold) and ate a can of cold tamales for dinner..
With
cold water to wash it down.. Yum..
Went to
bed early since there was nothing else to do... Power was back on about midnight or so..
Happy to
be home and looking forward to the surgery..
I understand that they go in through the front and I need both sides
done so they will be cutting my throat..
2002
will be a good year..
Rick
Draganowski
Subject: Medical Road Trip part II and Rustpuppy
Date: Tuesday, January 08, 2002 8:37 PM
I got the
numbers for the Suburban milage on the homeward trip against the hurricane
wind.. It was pretty good
considering the weather issues at 17.72 mpg.
With the trip to Medford at 19.92 mpg it comes to a trip average of 18.71
mpg.. I love that old Suburban...
Now for
something entirely different.. I
started Rustpuppy up and let her idle aand warm up at about 10:30 this
morning.. I wanted to take her out
on the road.. At first I had no
intentions of doing anything except a nice drive in the country.. The Sunday/Monday storm dropped almost
exactly one foot (12”) of rain in the area and the roads will be wet for many
days..
But it
was such a pretty sunny day, and the road didn’t seem that bad..
And
there was no traffic at all..
So I
lined her up on the south end of Rustpuppy Run for a northbound run.. I picked the best launch spot I could
find.. But the wheelspin was too
much, all through first and about a third of the way into second gear..
Rustpuppy
was fishtailing so much it was like she was doing the hula.. I was so busy steering and the shift light
came up much quicker than usual so I was slow on grabbing second. As a result Goody wound up to about
6700rpm.. Goody sounded great at that
rpm with no valve float or ignition issues..
But it is probably overstressing the rotating parts.. I need faster reflexes..
Anyway
the time was better than I expected because Goody was pulling so well at the
top end so the numbers came up 14.26@106.8...
We are
due for three more dry days so I am looking forward to getting in some more
runs as the road dries out..
More to
come..
Rick
Draganowski
Subject: Rustpuppy Test&Tune 76
Date: Monday, January 14, 2002 10:39 PM
Sunday
morning dawned clear and dry.. By the
afternoon the dry light winds and the bright sunshine had finished the work on
drying highway 101..
With
suppressed eagerness I fired up Rustpuppy at about two in the afternoon to take
a little ride..
I got to
the north end of Rustpuppy Run without any nervous practice runs because I
planned on taking my time and making several runs.. Due to some flukes of traffic there was no interval long enough
for a safe southbound run so I found myself on the short turnaround on the
south end of the Run..
I nosed
Rustpuppy up to the edge of the highway so I could see down the highway
southbound to look for a good long traffic break. Normally I would tear out onto the highway at full throttle up
to about 4500rpm (about 86mph) to get to the south staging area.. But there was the front end of a car parked
up the road that made me uneasy.. I
considered my options and almost went ahead with the run to the staging area
but decided to turn south and investigate the parked car..
My
instinct was a good one.. It was a
ratty old Oregon State Police Crown Victoria staking out the highway and with a
clear view of where I would have done the practice launch.. I turned off onto the old road and tried to
look as innocent as possible while sneaking off back home..
Whew.. I would have been nailed good.. And there is more to the story..
On the
way home I was innocently fooling with the shifter and I noticed that it was
not working correctly.. The
downshifts seemed ok but the 2-3 upshift was fouling up 3 times out of 4..
So if I
had gone ahead with the racing with the shifter fouled up I may have seriously
overreved Goody and caused myself serious grief..
The
rains came back last night so the temptation of the open highway is back on
hold.. I doused the shifter with some
great spray on penetrating oil with magic ingredients and Teflon and it is back
to normal. Its upshift pawl was
sticking due to surface rust.. The
salt air syndrome again.. Will take a
picture of the super penetrating oil tomorrow.. I am so fuzzy I forgot the details.
More to
come..
Rick
Draganowski
(happy to
avoid entanglements with the law)
Subject: Rustpuppy Racing and Construction Report
Date: Monday, February 04, 2002 1:28 AM
Chuck
Butcher and his assistant Donny Davis showed up last Tuesday at 8:30 pm for the
big barn project here..
But
first about the racing.. Chuck and Donny
got a ride in Rustpuppy Wednesday when I took them to town to introduce them to
my supplier, Reed Ringer at Gold Beach Lumber.. And then the road dried enough to give me some ideas yesterday
(Saturday) so I got back from an errand to town in the Suburban and immediately
got back on the road with Rustpuppy..
The weather was almost perfect (with a little more wind and pavement
moisture than ideal but still good) and I was itching for a Rustpuppy Run as it
has been since January 8th since the last run. (and it was a bad one on wet road) The State Trooper and the shifter rust put
the kibosh on the attempt on the 14th of January and I have spent
about 3 weeks recovering from almost knocking my brains out on Junkyard Dawg..
I did
one practice 0-60 run on the old road and had the reasonable cold motor time of
4.9 seconds.. It was time to hit the
Run..
Too much
traffic to allow a southbound run so I set up for a northbound one. The launch area was too wet for optimum
traction so the initial wheelspin seemed interminable.. But Goody was pulling well up through the
gears and the run was a most satisfying 13.63@109.2.. The high mph was partly due to the tailwind
and partly because of the great way Goody was pulling in the higher gears..
This is
quarter mile run number 101 since Goody was installed.. What fun..
Now back
to the construction report.. Attached
are a few selected pictures of the progress.. First is the rig that Chuck drove over from Baker City (600
miles).. Then some construction items..
Rick
Draganowski
(good progress
is being made)
Subject: Weather and Rustpuppy racing and tach issues
Date: Friday, February 08, 2002 6:05 PM
Naturally
since we are in the middle of a construction project with siding off and walls
open a unexpected severe Oregon winter storm hit yesterday afternoon..
Local
winds of over 90mph and about 4 inches of rain.. It was an exciting time for us all.. Naturally I went to town during the worse of it.. But it was in the Suburban.. No problem..
Today
started with showers and then became a great sunny day with light winds and
about 55 degree temperatures..
So due
to my restless nature and need for mood elevating speed I took Rustpuppy out on the saturated
highway.. To my surprise I found a
dry patch down from the north end of Rustpuppy Run and managed to get a decent
launch.. The 1-2 shift happened on the
wetter part and caused momentary concern due to a sudden jog to the right by
the rear end. It was not severe enough
to cause me to let off so the run progressed well..
Without
the tailwind Rustpuppy had last run the mph was more normal and the time was
very good at 13.59@107...
On the
return morthbound trip I could not find any unsaturated launch area and just
tried a 0-60 run for the fun of it..
There was wheelspin through all of first gear and the time was off at
5.3 seconds.. Even with the wheelspin
Rustpuppy was still pulling pretty good and it was great fun..
Tomorrow
will be dry and sunny and I may unload the 87lbs of trunk junk and have another
go at breaking the 13.5 barrier with the bumpers on..
But, (another damn but) the fun was a little
spoiled by the Sun Super Tach II failing..
And after only 10 years of service..
It seemed to hit something internally and would not go above 2000
rpm.. Then after the racing it was ok
up to about 3000 rpm... I think one
of those damn spiders may have spun a web inside.. Another arach-tach problem..
I have
the new tach (almost identical) on the old test stand used for Goody and will
probably do the transplant this weekend..
Just wirenuts and the single rear mounting ring..
The
construction is going good and there will be an update Sunday or so..
More to
come..
Rick
Draganowski
(racing is
good)
Subject: Rustpuppy Test&Tune 77
Date: Monday, February 11, 2002 10:50 AM
The
saturation of the highway from last Thursday’s storm had been mostly dried by
Saturday and I went ahead with the idea (or was it a threat) of testing
Rustpuppy with the great winter gas and the 87 lbs of trunk junk removed..
About
the gas.. The last time I filled
Rustpuppy the lady who was pumping gas was a new hire and despite my request
for 92 octane she filled Rustpuppy with the bottom of the line 87 octane
regular.. (she probably judged
Rustpuppy by her shabby exterior looks)
Strangely,
with the quality winter gasoline and cool winter weather Goody seems happy and
runs great on the 87 octane stuff.. With the milled heads and thin shim head
gasket her compression ratio is right at 9 to 1 so perhaps regular gas would be
adaquate. (if the quality of the
gasoline is high)
I
invested in a couple sets of R44TS plugs to replace the R45TS jobs in Goody now
since on hot days there is a tiny bit of dieseling when shutting down after
climbing the grade up the back side of Colebrook Butte where I live.. But I have been to lazy and distracted to
get them installed.. Will probably do
it before switching back to 92 octane to see what the plugs think of the
regular gas..
But back
to the racing.. Saturday I unloaded
the 87 lbs of trunk junk and warmed Rustpuppy up for a run..
On the
practice 0-60 run on the old road the time was fair at 4.84 seconds so I was
encouraged. The highway looked dry
after a couple days of low humidity and sunshine but the traction issues were
still serious on the southbound run.
The wheelspin was way out of line with the miserable time of 14.11@102.8 on the G-Tech.. I think the asphalt is porous and it
takes a while to get the water table inside down below the surface far enough
to allow decent racing traction..
The
northbound run was much better but there was still too much wheelspin in first
gear. The lack of ballast in the trunk
is also a traction factor.. It would be
a much better test to pull the front bumper assembly.. The paranoid reaction I had to the
Mustang T-Bone Incident is fading and twisted thoughts of de-bumperizing
Rustpuppy are emerging.
Anyway
the northbound run was very good at a flat 13.5@108
on the G-Tech.. Everything on Rustpuppy
is working well and it is a great tonic to be able to tear up the highway like
this..
Sunday
was another dry sunny day with light winds but late in the afternoon I could
see clouds approaching ofshore. Perhaps
bringing some drizzle. That would end
the hotrod crazy behavior for a while..
With the
87 lbs of trunk junk back in Rustpuppy and the gas tank a little less than half
full I set out to make another series of runs.. The 0-60 practice time
was better at 4.77 even with a slight cold motor bog so I was encouraged..
Out on
the highway I had a fair southbound run with a more than moderate wheelspin
since the traction at it’s best here is not as good as the other end of the
run. The time was 13.58@107.1 on the G-Tech.. I knew that the northbound run would be
better..
It
was. Everything came into place with
just enough wheelspin at launch to get Goody up into the powerband of the XE268
cam.. The G forces at launch were
enough to blow back the sun visor on the driver’s side. (that is how I know that the tires hooked up)
The time
was most excellent for the fully loaded configuration of Rustpuppy at 13.44@108.4 on the G-Tech! That is only 2 hundredth’s more that
Rustpuppy’s best time with the bumpers off and trunk junk out.. The winter gasoline makes a big difference..
Now I
have twisted plans to remove the front bumper and perhaps get Rustpuppy into
the 13.3’s.. And thinking sick
thoughts about cheap lift-off fiberglas hoods.. And I still have the exhaust cutouts to install... Hmmm... 13.2’s??
More to
come...
Rick
Draganowski
Subject: Rustpuppy Test&Tune 78
Date: Tuesday, February 12, 2002 6:34 PM
Yesterday,
Thad Bell, my good friend who currently lives in Belgium brought up the subject
of when I was going to give Chuck a racing ride on Rustpuppy Run.. I had mentioned that he was invited to
join me on any race day when he first arrived. But due to the press of events he forgot the invitation and I
had been politely waiting for him to accept.
He on the other had had been politely waiting for me to ask..
It was a
comedy of errors and I am glad that Thad said something..
Turns out
that Chuck was eager for a Rustpuppy Run and this morning we set out for one
together..
The
warm-up 0-60 on the old road went well with the nice time of 4.82
seconds.. Considering the extra 150
lbs (Chuck is a slender fellow) it was excellent..
The press
of traffic prevented a southbound run so we turned around and set up for a
northbound run.. The launch was below
standard with a little more wheelspin than I expected.. I expect that I may have missed the ideal
launch area by a few feet on staging..
The run
went well but due to the appearance of an on-coming car I braked more than
usual after the run (about 110mph down to 60) and Chuck took exception to my
style. It was necessary to brake so
that when the oncoming car drew near we would be back within reasonable
distance from the speed limit..
Anyway
the time was fair at 13.69@106.9 and Chuck was
happy to have been aboard.. He says
that he has been missing racing a lot..
I
suspect the mph is down due to me instinctively letting up on the gas when the
oncoming car came into view..
Perhaps
if the weather stays dry we will try again..
More to
come..
Rick
Draganowski
(old farts
having fun)
Subject: Rustpuppy Test&Tune 79
Date: Friday, February 15, 2002 9:21 PM
Yesterday
(Valentine’s Day) morning I started
making good on the threats I made in Test&Tune 77. Taking advantage of the springlike weather I
crawled under and removed Rustpuppy’s front bumper.. Hehehe... The bolts
have been polished and oiled and only three on each side are being used so it
only took a few minutes.. But the press
of work and the inevitable problems of rebuilding ancient buildings interfered
with racing plans till just before sunset..
Rustpuppy
felt perky without the heavy disco front bumper and had the practice 0-60 time
of 4.59 seconds.. The old road was
still bone dry but since Goody was still cold there was a trace of bog..
Out on
Highway 101 closer to the ocean the misty haze was setting in and the humidity
was climbing rapidly.. Traffic was
spaced to interfere with a south bound run and by the time I got to the south
end staging area the fog was closing in quickly..
I tried
a run anyway but had too much wheelspin off the line and again into second gear
to make a good run.. But the time was
pretty good anyway at 13.5@108.6 on the G-Tech..
Then an
uncanny and upsetting thing happened on the way home.. Just before getting to my place Goody
started making the most unusual whirring scraping noise..
My
stress hormones shot through the roof as I visualized innumerable horrible
scenarios that would cause a motor to make strange noises.. If I have blown up Goody by my “drive it
like you stole it” habits I would be discouraged... A dark and somber moment..
After I parked
Rustpuppy and went down to where Chuck was working he mentioned hearing a
strange noise from Rustpuppy when I pulled up.. Damn... What a revoltin
development..
I went
back and started driving Rustpuppy gingerly around in the yard listening to the
ghastly whirring scraping grinding noise..
Donny Davis, Chuck’s assistant, was watching with his sharp young eyes
and noticed something strange sticking down under Rustpuppy. He motioned for me to stop and reached
under and came up with an 18” long piece of tree branch that had bounced up and
entered the hole in the flywheel cover by the starter and was rubbing on the
flexplate and torque converter in there..
What a
strange business.. It was a vast
relief to find that the horrible noise was just an out of place twig..
Thank
you Donny Davis..
It would
have been a nasty experience to pull Goody out to find a stick in the flywheel
cover..
Rick
Draganowski
(need to
sweep the road of the storm debris)
Subject: Rustpuppy Test&Tune 80
Date: Wednesday, February 20, 2002 8:42 AM
I aked
Donny where the stick that he extracted from the flywheel cover was.. He had the good sense to save it and the two
pictures attached show the devilish thing..
It really gave
me a bad few minutes..
I took
Rustpuppy out for a confidence building run the next day but due to the light
rain we had overnight I did not expect good traction or times..
I was
right.. The wheelspin was back in the
damp road range and the time on the G-Tech was 13.58@107
. It has been raining since then
(the morning of the 16th) and there will be no reasonable racing
till the dry weather returns..
But it
felt damn good to have Goody running so sweetly without any strange noises..
More to
come..
Rick
Draganowski
Subject: Rustpuppy Test&Tune 81
Date: Thursday, February 28, 2002 7:58 PM
It has
been eight days since a Rustpuppy racing report.. Combination of reasons including weather, stomach flu, serious
construction project business, and scratching up the dough to pay for the
construction project.. But I been
running the daylights out of Rustpuppy when I could..
On the
23rd the weather had been miserable the day before with drizzle and
cold fog but it eased up that morning and I took Rustpuppy out for a run.. The barometer was down after a dry cold
front and the traction was bad but Rustpuppy still was able to pull the
reasonable time of 13.65@106.7 on the G-Tech..
After
two clear and sunny and dry days with low humidity I ignored my stomach flu
enough to get out for some racing..
This was the morning of the 26th. (day before Chuck was
leaving) The 0-60 time with a cold bog
was 4.67 seconds.. The southbound run
started with a slight bog and was against a headwind of about 10mph but I found
the good traction spot and Rustpuppy pulled the excellent time of 13.46@107.8 ..
The
transmission fluid was warmed up and the stall speed of the converter
went up
on the northbound run so the wheelspin in first gear was pronounced.. The time was still great at 13.47@108.6 with the wind and in spite of the
wheelspin.. It felt so good I bet it
would have been a 13.3x run with a bit more traction..
Still it
is pretty good times on plain old BFGoodrich Radial T/A tires.. (245/60-14)
That
evening after we went through the Novalist mail I noticed that it was clear and
dry and windless.. I talked Chuck
into riding along for another blast down Rustpuppy Run..
We made
just the southbound run and it went splendidly well for a time of 13.5@107.8 with Chuck aboard.. He said that he enjoyed it
immensely.. So did I..
Yesterday
Chuck left at about 8:45 in the morning and I was getting over my stomach flu
and went to town on business leaving John cleaning up after the construction..
That
evening just at dusk again I noticed that the wind had died out..
Cool..
Only
about 5 gallons of gas left in Rustpuppy but enough for one more blast..
The 0-60
time on the old road was fair at 4.69 with the bog..
The
southbound run was the first one that felt perfect in a long time..
The
results tied Rustpuppy’s best time..
It was 13.42@108.3.. Hoo haa! I love it when it seems perfect..
Northbound
run with the converter stall up from the heat had enough wheelspin in first
gear to drop back to a respectable 13.5@107.6
...
Today it
was much too windy to even think about racing.. Gusts to 30mph..
More to
come..
Time for
an oil and filter change and a complete inspection of Rustpuppy.. (I am a little paranoid from seeing Shawn’s
reports) Have her up on ramps in front
of my beautiful shop.. See picture..
Rick
Draganowski
(driving
Rustpuppy like I stole her)
Subject: Rustpuppy Test&Tune 82
Date: Sunday, March 03, 2002 12:18 PM
With
Rustpuppy conveniently up on ramps I busied myself with the oil change and
inspection.. This view
(t&t82-1.jpg) is one of the pretty angles to look at Rustpuppy..
Everything
checked out as far as the inspection goes except one thing.. I had noticed a drop in oil level in Goody
and it looks like the front seal is leaking slightly.. No explanation of that since it was a new
(Proform) vibration damper going into a new seal on a new motor.. And I did put a little grease on the damper
to prevent snagging the seal..
Hmm.. See t&t82-2.jpg...
The
closeup (t&t82-2x,jpg) shows the damper is not slipping at all..
The line between
the silver and blue paint is still as it was when painted.. But the sliver paint is not holding up to
the salt air.. Sigh..
Since
the antique Sun tach on Rustpuppy quit working about 2 months ago I planned to
replace it with the new tach from the Goody Test Stand.. (t&t82-3.jpg)
The swap took just a few minutes since the old tach was
installed with wirenuts to allow quick installation of the shiftlight..
The next
day the wind had died down and it was much warmer.. About 70 degrees! I had
John get some gasoline from town for the mower and Rustpuppy but instead of
following directions to get the regular gas from Chevron he got the middle grade
gas from Union 76.. I put about 3
gallons of it in with the 2 gallons of Chevron regular left to provide enough
for some racing..
The run
went ok with the time of 13.59@107.3 but Goody
seemed a little flatter than normal and the time was well over a tenth down
from expected..
The
combination of the almost 20 degree rise in temp, the higher viscosity oil, and
the different gasoline probably added up to the difference..
One
thing I noticed was that the new (bought in 2000) Sun Super Tach II was useless
for racing.. They had cheapened the
design to cut costs and the result was so much lag in the needle compared to
the real rpm as to make the readout meaningless.. Goody could rev to the 5800rpm shift light speed so much
faster than the new tach could respond that it indicated less than 3000 rpm
when the light lit.. Bah!
Have to
fix my antique tach (bought in 1994) or get a better quality one..
Being
broke I dug into fixing the old one..
The spider had really done a
job on
it. See t&t82-4.jpg.
I broke the brittle
old redline indicator
plastic
needle but managed to get the spiderwebs cleaned out and the tach
reassembled.. I don’t need the
indicator with the shiftlight keeping me informed. T&t82-5.jpg shows the tachs passing on the seat during the
swap back..
The
disintegration of the temporary
upholstery fix on the drivers door panel had been bothering me for some
time.. The ends of the duct tape were
hanging down below the door and flapping in the breeze while driving.. A couple of weeks ago I bought an upholstery
repair kit at NAPA.. You can see it
posed on my latest Jeg’s catalog in t&t82-6,jpg.
The
rather nasty appearance of the door before is portrayed in t&t82-7.jpg and
the spiffy look after in t&t82-8.jpg..
The
closing picture captures the elegance of the Rustpuppy cockpit with the overall
leg with duct tape trim boot on the Pro-Matic shifter and everything as it
should be.. See t&t82-9.jpg.
More to
come..
Rick
Draganowski
Subject: Rustpuppy Test&Tune 83
Date: Sunday, March 17, 2002 7:33 PM
It’s
been two weeks since the last report and the weather has been miserable.. First about 3 feet of rain followed by the
biggest nasty cold front with continous sleet and hail showers for days with
temps in the low 40’s..
But
today the sun came out and the showers got spotty.. I bailed out the water that had accumulated in the floor pans
of Rustpuppy from the cosmetically challenged body features..
There
was about 3 or 4 gallons of cheap mid grade Union 76 gas left so I put in five
gallons of Texaco 92 octane premium stuff..
I
decided to take Rustpuppy for an innocent little ride just to get some seat
time and keep everything working..
With the wet roads and the variable gusty cold winds it was not a good
idea for any racing.. Especially with
the front bumper off and the nose high gasser look with the miserable
aerodynamics..
On the
north end of Rustpuppy Run I noticed that the wind had mostly dried the patch
of good pavement and there was no traffic..
The wind was gusting toward the wide side of the Run so I couldn’t hold
myself back and staged for a run..
Goody
wasn’t fully warmed up yet so there was the slightest bog at launch which
controlled the excessive wheelspin I expected from the waterlogged
asphalt.. The run went fairly good
with a noiseless wheelspin wobble into second from the wet road and a
considerable amount of steering corrections needed due to the wind gusts.. The report from the G-Tech showed 13.55@107.4 which was most satisfying..
I have
been a bit depressed the last week or so and this racing (even ill-advised) is a
great anti-depressant..
Goody
seems happy with the winter Texaco 92 octane..
Later I
went to town for an appointment in the Suburban.. I love that old monster..
A Datsun pick-up with a load of firewood was motoring along in front of
me at about 45-50mph and when I got a chance to pass I floored the Suburban and
took off..
The
sweet sound of the Goodwrench 350 downshifting from 4th into second
gear and winding up echoed from the 3 inch bus muffler and added some more
cheer to my existence..
More to
come..
Rick
Draganowski
(fun with
old cars is good)
Subject: Rustpuppy Test&Tune 84
Date: Thursday, March 21, 2002 12:59 PM
The
weather has made a complete recovery with sunny skies and 60 degree temps and
it looks like Old Man Winter has left town..
Tuesday I wanted to make a few runs to properly test the 92 octane
Texaco gas now in Rustpuppy..
The
first run southbound was perfect with perfect traction and a little
headwind.. The time was off from the
previous tests with 13.53@107 but still good..
The second
northbound run started good but when traffic suddenly appeared ahead I think I
instinctively lifted on the throttle..
The time was way off at 13.91@106.4..
Problem
was I couldn’t remember whether I lifted or not.. So I started worrying that something may be going wrong.. Rustpuppy is up to 119 quarter mile runs
on Goody at this point..
Next day I
set out to see if anything had gone off..
Traffic was thick but after waiting for a break I managed a southbound
run from the good patch of asphalt.
Time was ok at 13.61@106.9 but now I am
convince that the slower burning of the premium (from the octane enhancing
additives) reduces peak combustion pressures and Goody is down on power.. Can actually feel the slight difference
in torque going up through the gears..
A seeming lack of the eagerness that she has with the regular 87 octane
gas.. The outside temperature was up
about 10 or 15 degrees since yesterday as well..
I worked
in the shop at the milling machine most of the day (and my bones
were
creaking) and late in the afternoon I decided to go to town for
groceries.. I have been chicken and
squeamish about getting the neck surgery and have been rationalizing delays
since last December.. But the
symptoms are getting damn bad and the time has come.. I stopped at Doc Williams office and started the ball rolling
with a Monday appointment..
Later
after shopping and a business meeting it was time to cruise home in the
Suburban. It was just before dusk and
the wind had stopped completely.. The
temperature was down and the sea was smooth as glass.. I started getting worked up about making a
late evening run with Rustpuppy and raced home to beat the evening condensation..
I left
the groceries in the Suburban and jumped into Rustpuppy and zoomed down the
hill to Rustpuppy Run.. I was in a
hurry to get going since I knew that I only had a few minutes before the
moisture condensing on the pavement destroyed the traction..
I staged
on the nifty patch of launching pavement on the southbound run and took off
with a perfect launch.. The cooler air
made a difference.. The run was
flawless and Goody was pulling great..
It should be a below 13.5 run..
But, (why is there always a but?)
The old
idiot Draganowski in his haste to launch didn’t wait long enough for the G-Tech
to initialize and flash Go..
Duh.. For the first time I
red-lighted the G-Tech and took off too damn soon.. Duh again.. Run went great
but I was worried that the timer was still running and I was approaching
redline in third gear.. That is about
115mph.. And when the time came up it
was ridiculous at 14.81@92.7.. Duh again..
By the
time I got down to the south turnaround and back on the northbound launch area
the condensation had started and the wheelspin spoiled the last run of the
evening.. More than half of first
gear was spinning for a time of 13.73@106.3..
One
thing proved though.. The 92 octane is
slower by about .15 seconds and 2 mph than the regular gas..
Up to
122 quarter mile runs now..
More to
come..
Rick
Draganowski
(they are
gonna cut my throat.. sigh..)
Subject: Rustpuppy Test&Tune 85
Date: Saturday, March 30, 2002 7:32 PM
For the
last 8 days or so the weather has been amazing.. Sunny and 60 something degrees every day.. The roads have dried completely and you
would think that it was time for some racing..
But the
incredible northwest wind has been blowing every day insanely.. Gusting to about 30 mph crosswinds on
Rustpuppy Run so ol’ Draganowski has been too chicken to do any running..
About 5
days ago I ran the last of the winter 92 octane out and got 5 gallons of the 87
octane regular into Rustpuppy.. But I
think it is too late and the summer blend is starting already.. No way to tell without running..
Today
for the first time the wind seemed to be moderating so I got Rustpuppy out for
a shot at the Run..
The
practice 0-60 was just ok at 4.85 seconds..
Goody was still cold..
The wind
up at my property was much lessened but down on Rustpuppy Run it still seemed too strong for a comfortable ride..
About
15mph from mostly north down Rustpuppy Run..
Enought from the west to make it interesting though..
The holiday
traffic was much more than I expected and there was no opportunity to make a
southbound run.. But a break opened
up and I staged for a upwind northbound run.. Traction seemed good but the wind was gusting more than I
expected and Rustpuppy was giving me the front end floating feeling at the top
of the run.. The airspeed was probably
about 120mph and with the front bumper off nose high trim it was an unsettling
feeling..
The run
was fair considering the headwind at 13.56@106.7
on the G-Tech...
I was
bummed out by the traffic and floating feeling and decided to call it quits for
the day..
But
later, just a little after six o’clock I noticed that the whitecaps on the sea
had ended and the air was still.. The
sun was setting and the temperature was dropping but I knew I had time for
maybe one or two runs before the condensation started..
I zoomed
down the old road and grabbed a quick 0-60 practice time of 4.74 seconds..
Traffic was
done for the day and the wind had stopped..
I staged on the good patch for a southbound run and everything seemed to
be working for a nice stable run. The
run was a good one but the times were off the pace of the winter gas with a 13.48@107.5 on the G-Tech.. About a tenth and one mph off of the
goodest runs..
By the
time I got turned around for a northbound run I could see that it was probably
too late to retain the dry traction..
I was right. Way too much first
gear wheelspin for a time of 13.61@107.5..
But it
was a happy experiment and it looks like it is time to go back to the summer 92
octane , put the front bumper back on, and get serious about adding some power
to get to the next stage..
I am
betting that the cutouts will make up for the bumper and summer gas and get
Rustpuppy back into the low 13.4’s or mebbe high 13.3’s..
Then it
will be time to take the bumper off again..
More to
come..
Rick
Draganowski
(waiting for
word about surgical schedule)
Subject: Rustpuppy Test&Tune 86
Date: Sunday, April 07, 2002 7:43 PM
Last
Thursday I had my helper John Spada put Rustpuppy’s front bumper back on.. I made a trip to town with Rustpuppy while
the Suburban was in the shop so the tank was filled with 92 octane intermediate
blend (not the goodest winter stuff) Texaco gasoline..
The
weather was reasonable so I took the fully laden Rustpuppy out for a run.. Everything went good on the practice 0-60
for a time of 4.9 seconds with a bit of cold bog..
The
southbound run went very well with plenty of traction from the full gas tank
and came up with the moderate time of 13.65@106 on the G-Tech..
Adding
the 84 lbs of the front bumper assembly and the extra 16 gallons of gas at
about 96 lbs really is loading Rustpuppy down..
On the
way back on the old road I did a few traction tests to check maximum g-force
generated.. It varied from about 0.7
to about 0.85 g’s..
On one
spot there was radical wheelspin with smoke which took me by suprise.. Later I noticed that I had launched on a
spot of raw tar on the road and melted two groves into the pavement.. Cool..
You can see the polished tar surface reflecting the sky in the
pictures.. Looks like it will be a
permanent burnout mark.. See
t&t88-1.jpg and t&t86-2.jpg..
The
Suburban is in the shop getting front wheel bearings and brake pads and new
rotors.. Also a strange exhaust leak
showed up on the stock manifold and getting it all fixed cost about 400 bux.. Damn..
But I love that old urban assault vehicle..
Today I
decided to just take an innocent little ride in Rustpuppy as the wind is too
strong for serious racing.. Lots of
traffic on the southbound part of the run but I noticed that the wind was
mostly aligned with the run for a direct headwind on the northbound run..
What the
heck.. There was a break in traffic
and the launch went good with plenty of traction from the full tank.. With the front bumper in place Rustpuppy
is slightly nose down so she tracked nice and steady against the 15-20mph
headwind.. No lifting or floaty feelings..
Cool.. The time was way down
from the wind at 13.71@105.7 and something
unpleasant happened at the top of the run above 100mph..
A nasty
irregular snapping/slapping noise started suddenly and my paranoia surfaced in
full flower.. I have never heard
anything like it and was going nuts trying to figure it out as I slowed
Rustpuppy down focusing on the road ahead..
Out of the corner of my eye I detected movement and a quick glance to
the right showed the stupid top outside window fuzzy whipping in the wind and
slapping the hell out of the passengers side window..
What a
relief.. Stuffed it back in place
when I got home and will glue it in tomorrow..
I hate
strange noises when I am racing the piss out of Rustpuppy..
More to
come..
Rick
Draganowski
Subject: Rustpuppy Test&Tune 87
Date: Tuesday, April 16, 2002 3:39 PM
After
getting the components made I installed the new Pyrometer system in Rustpuppy
on Sunday.. Then find out that I had
left the headlights on from the last seat time episode last Friday. The battery was a flat as it can get..
When I
put the charger on it acted funny..
(I had it hooked to the stud on the alternator since the battery is in
the trunk)
Goody
seemed to start ok after an hour or so of battery charging but the voltage
gauge seemed to be indicating voltage too high for a flat battery..
Anyway I
took off for a test run of the Pyrometer..
We had about 4 inches of rain on Friday night and Saturday so the road
was not suitable for racing but I pressed on regardless..
The
Pyrometer system was working well but Goody seemed flat.. Not pulling like normal.. I staged on the best spot of the southbound
Rustpuppy Run and pulled less wheelspin than I expected.. The time was way off at 14.01@106.6 and I was beginning to worry that
something was wrong..
The
northbound run was miserable with wheelspin through most of first gear but
still Goody was not pulling right at higher rpm.. I couldn’t put my finger on it but something was seriously
wrong since the time was 14.09@103.4.. Even with the wheelspin the speed was way
off..
Thinking
that the mostly flat battery was somehow to blame I decided to put the charger
on the battery itself in the trunk and leave it overnight for a proper charge..
I found
that the cheesy clamp on side terminal battery connector was blown out.. The nut had pulled out of the clamp and the
cable was just barely making contact to the terminal.. Not good at all.. I think that running without the battery properly connected did
weird things to the MSD distributor and resulted in the high rpm power loss..
Also I
noticed that during the racing the exhaust gas temperatures were down about 200
degrees from what I expected (and have seen before)..
Attached
and in the addendum are pictures of the Pyrometer installation on Goody and the
reading after the racing.. Note that
Goody is still running in the pictures and that the high temp telltales show
what the peak tempratures seen during the racing..
These
runs (sad as they are) bring the total number of quarter mile runs since Goody
was installed in Rustpuppy to 129..
Some fun..
More to come..
Rick
Draganowski
(fixing the
battery cable today)
Subject: Rustpuppy Test&Tune 88
Date: Thursday, April 18, 2002 1:41 AM
More
excitement today (Wednesday) as the cold rain showers eased considerably so I
took Rustpuppy out for another run with the repaired battery cable..
Traction
was going to be an issue but I wanted to see if there was any difference in the
Pyrometer readings with the repaired battery cable.. The first (southbound) started with a small cold bog so the
wheelspin was not out of control but still about a quarter of a second was
lost.. The time was reasonable at 13.83@104.1..
It would have been in the 13.6’s on a dry road..
The
northbound run was out of control with the wheelspin through most of first gear
and with another bout of wheelspin at the start of second gear.. The time was not quick at 13.92@105.6 with the speed going up.. Another southbound run would have been
better but the evening traffic was building up and I decided to call it quits
for today..
The
pyrometer readings were almost identical to last time with the max readings
between 1400 and 1200 degrees.. The
picture was messed up from the reflection of the sky.. See t&t88-1.jpg..
T&t88-2.jpg
shows the trunk mounted battery in Rustpuppy with the new positive
terminal..
Now I should swap out the sorry clamp on terminal on the
ground lead..
T&t88-3.jpg
shows the blown out clamp on terminal and the copper lug solder-on replacement..
More to
come..
Rick
Draganowski
(131 runs so
far)
(waiting
impatiently for the roads to dry)
Subject: Rustpuppy Test&Tune 89
Date: Saturday, April 20, 2002 2:32 PM
Yesterday
the showers ended and the roads started drying out but the damn coastal winds
started back up.. (that evening it was
gusting to 40knots in Gold Beach)
I took
Rustpuppy out for a run about one in the afternoon.. I just wanted to get another baseline on the Pyrometer
system.. The wind was strong (about
25mph) but almost exactly from the north and lined up with Rustpuppy Run..
Too much
traffic for a southbound run so I turned around and set up for an against the
wind northbound run.. There was
enough moisture still left in the road to cause too much wheelspin in first
(about half way through up to about 25mph)
so I didn’t expect a very quick time..
Rustpuppy
was tracking well with the front bumper back on, half a tank of gas, and the
new ESPO rear springs causing a slight nose-down attitude at speed.. I decided to stay on the gas (being sure to
leave enough room to slow down at the end) through most of the 7 tenths mile
long Rustpuppy Run..
The tach
was up to 5800 rpm in 3rd gear when I had to let off to get slowed
down for the turnoff.. That works out
to about 114-118 mph depending on converter slip and tire growth factors.. Against the 15 mph headwind the air speed
could have been as high as 133mph..
Not too much lift and the tracking was steady but it would have be
foolish to try this with any sidewinds..
The
G-Tech time was 13.82@105 but the most interesting
part was the max readings on the Pyrometer..
Here they are.. At the far right
are the last max temps recorded with a different Pyrometer system and with the
good winter gas..
Cyl Temp
old Temp diff
1 1425
1425 0
2 1375
1490 -115
3 1500
1470 +30
4 1450
1300 +150
5 1280
1410 -130
6 1380
1525 -145
7 1380
1525 -145
8 1380
1475 -90
Interesting
data but difficult to interpret..
Cylinder number 4 is strange and I suspect that the original number 4
thermocouple may have been screwed up..
More to
come..
Rick
Draganowski
Subject: Rustpuppy Test&Tune 90
Date: Saturday, April 20, 2002 9:48 PM
Today
the wind was really nuts and I gave up on the idea of doing any Rustpuppy Runs.. I ground away at several projects in my
office till after six.. I ran across
many items of paperwork that reminded me of my Deloris.. I was getting pretty depressed by quitting
time..
Then
when I was washing up before going in I noticed that just as the sun was
setting the wind died to nothing..
Hmmm.. I only had a few minutes
before the evening condensation would come down..
I raced
out to Rustpuppy on the lawn tractor and fired her up and took off in a blast
of bogging acceleration to get to Rustpuppy Run..
I
figured I was just in time for a perfect southbound run.. The 0-60 warm up run was fair at 4.84
seconds.. But just as I got staged
on the perfect piece of asphalt for a southbound run an oncoming car cleared
the curve at the south end of the run..
Damn..
I
whizzed Rustpuppy down to the short gravel turnaround and waited for traffic to
clear again.. Then took off
at full throttle to get to the northbound staging area..
Traffic
all clear. Rustpuppy took off with a
little more wheelspin than optimum but not too bad.. I stayed on the throttle after clearing the quarter mile and
clear up to 6000rpm in 3rd..
Somewhere between an honest 120 and 122mph.. Without any headwind Rustpuppy felt great at that speed.. Smooth and steady..
I jotted
down the G-Tech time after I turned off on the old road.. Pretty good time at 13.65@106.7..
Without that wheelspin in first it would have been a 13.5x run..
I quickly
turned around for a blast at the southbound run.. But it was
too
late.. The launch on the perfect piece
of asphalt was poor with way too much wheelspin.. A real screamer..
The time indicated the amount of digging.. 13.99@106.7.. Same speed but bad e.t.
Since
the traffic was completely clear I staged for another northbound run but
feathered the throttle for a roll on launch because I expected wild
wheelspin.. That allowed a reasonable
time of 13.75@106.4.
Today’s
action brings it to a total of 135 quarter mile runs since Goody was installed..
I also
jotted down the Pyrometer readings..
The outside temperature almost 20 degrees cooler than during the run
yesterday..
1- 1425
2- 1340
3- 1500
4- 1390
5- 1300
6- 1370
7- 1390
8- 1370
Still a
little depressed but the racing helps..
More to
come..
Rick
Draganowski
Subject: Rustpuppy Test&Tune 91
Date: Sunday, April 21, 2002 11:08 PM
All the
talk about timing issues and Aren’s pinging problems inspired me to flange up a
piston stop so I can verify the TDC mark on Goody..
This
afternoon I messed about in the shop making it happen.. First I chucked up one of Craig Hauber’s
old AC R45TS sparkplugs in the lathe and turned off the crimp that holds the
porcelain insulator in the metal shell.
See t&t91-1.jpg..
Then
after measuring the hole in the shell I found it to be 0.338 inches.. The tap
drill size for a 3/8-16 thread is 0.3125..
Hmmm... Close enough.. It would provide about 50% thread form which would be plenty
for this application..
Then
after sticking the shell in the vise I attacked it with the 3/8-16 tap.. Using plenty of Cool Tool II lube.. (best I have ever found for tapping and
drilling) See t&t91-2.jpg
I
scrounged up some 3/8” allthread and a machine ball handle.. (cool, it had a brass insert threaded for
3.8”-16) I chucked the piece of
allthread in the lathe and polished a smooth end that would not scratch the top
of the piston.. The knob went on with
some Locktite Blue.. See
t&t91-3.jpg for this stage of the project..
The
addition of a lock nut to permanently locate the stop rod in the right
position
and allow installation and removal via the knob finished the
project
for today.. See t&t91-4.jpg
Small
projects that are easily finished in an afternoon are good..
More to
come..
Rick Draganowski
Subject: Rustpuppy Test&Tune 92
Date: Wednesday, April 24, 2002 11:05 PM
Lots of
strange behavior, interesting testing, and mental ups and downs over the last
two days..
It all
started yesterday... In the mid
afternoon on what has been the warmest day of the year (about 70 or so degrees
and little wind) I took Rustpuppy out for a run on what I know are the driest
roads so far this year..
I did
some traction testing (insane looking behavior as I rip off and then stop and
note the G-Tech readings) I did one
joyful full first gear burnout at the top of the hill and then when I rounded
the corner at the top there was a road crew loading a bulldozer on a flatbed trailer.. They all stared at me funny as I motored
innocently by..
Got down
to Rustpuppy run and staged on the very best patch of asphalt for a southbound
run.. Good launch but Goody seemed
flat.. Hmmm.. Time was really mediocre at 13.88@104.5..
Can’t blame it on wheelspin..
WTF?
Took the
Pyrometer temps..
1-1375
2-1290
3-bad
reading—open circuit- fixed today
4-1370
5-1270
6-1240
7-1280
8-1280
They
seem low? Hot air, less oxygen,
richer mixture?
I did
notice that Goody was up at 195 degrees after the full throttle bash..
And it
was almost hot down on Rustpuppy Run..
Wonder if
the underhood temp was this big a factor..
After I
got home I was just listening to Goody and sitting in the new gravel drive and
revving up to about 5000 rpm.. Sounded
smooth and sweet.. Later I noticed that
the downpointing exhausts had blown bald spots in the drive.. See t&t92-1.jpg..
Pulled a plug to check it but the high tech new premium
gas gives weird readings.. Sure didn’t look
rich though.. See t&t92-2.jpg..
Puzzled
over all of this strange information in my old head last evening..
On
another front I have been struggling with a bout of depression (mostly brought
on by the discovery that my arthritis meds are starting to cause nasty side
effects) and have been taking refuge in racing and aggravating the good people
on the list..
Last
night at about midnight I got a wild idea..
It was bone dry with no condensation..
No wind.. Almost full moon and
perfectly clear sky.. Temp down to
about 45 degrees..
Hmmm... What should I do? Right..
Go racing...
Jumped
into Rustpuppy and headed down to Rustpuppy run.. It has been several years since I have done any night runs and
the last time Rustpuppy was in the 15’s and 90something mph class.. It was a little exciting thinking about
blasting down the dark narrow run at well over a hundred..
Ran down
the old road but did no warmup runs or traction tests.. Wanted to get a cold start and then just
keep on racing to see what happens.
No
traffic at all.. Could have laid down
and taken a nap in the middle of Highway 101.. Staged for a southbound run on the perfect piece of
asphalt.. Plenty of time for a nice
relaxed run..
Took off
with just a hint of wheelspin and Goody felt like she was pulling good
again.. It seems much faster at
night.. What a ride!.. The time was much better at 13.63@107.5..
About as good as it gets with the bumper on and summer 92 octane.. Most excellent!
Turned
around and took a quick break to write down the results and get my pulse back
down..
Staged
on the best bit of asphalt for a northbound run.. More excitement and a good time of 13.67@107.2
on the G-Tech..
Another
break at the north turnaround and staged on the perfect piece for another
southbound run.. Little more
wheelspin as the stall speed is going up each run.. Still a rush to go this fast at night.. Stayed on the throttle up to 115mph just
for the hell of it..
Time was
down a little more at 13.7@105.9 on the G-Tech..
Final
run coming up.. Staged on the best
asphalt on the south end of the run but did a throttle roll on launch since I
expected too much wheelspin.. Time was
down a tad more at 13.75@106.5..
Very
interesting..
Pyrometer
readings were.
1-1425
2-1340
3-1470
4-1370
5-1280
6-1340
7-1380
8-1370
Goody
was only at about 170 degrees during the trip up the hill home..
What
fun..
This
afternoon I decided to try out my spiffy new piston stop.. I put Rustpuppy up on the ramps so I could crawl
under for the measurements.. See
t&t92-3.jpg..
I pulled
off the fan shroud and fan (see t&t92-4.jpg) so I could turn Goody with a
BF screwdriver wedged between double nutted studs on the waterpump..
If you tension the belt on the low side with your other
hand it gives the belt enough traction to turn the motor.. Gotta go slow due to the compression from
being lazy and leaving the other plugs in..
I had to lose the nifty knob on the piston stop tool due to interference
with the stupid headers at the number one spark hole.. Damn..
You can
see some of the tools lurking on the air cleaner in t&t92-5.jpg..
I made sure
Goody was sitting well below TDC on number 1 and pulled number one plug and
inserted the piston stop.. Set it
pretty deep as the lower the piston is stopped the more accurate the reading..
Turned
Goody one way to the stop, marked the damper at zero on the timing tab, turned
Goody the other to the stop, marked the damper again.. Then removed the stop, replaced the
sparkplug and rotated Goody till the TDC mark was pointing straight down..
Then it
was crawling my fat butt under to measure the marks with my flexible scale..
Results
were interesting.. The leading side
was 4.43 inches and the trailing side 4.3 inches.. Which means that the factory TDC mark on the new POS Proform
damper is about 0.065” retarded..
Since on an eight inch damper one degree is 0.0698” this means that the
mark is almost exactly one degree retarded..
In the
middle of this my neighbor Wayne Kreiger stopped by.. Wayne is an old friend who owns the ranch up at the top of the
hill.. He is also the Oregon State
Representative for this district..
Cool.. I showed him my office,
my projects, and we talked about politics and business and getting old.. It cheered me up considerable..
Threw
Rustpuppy back together and took her out for a spin.. Did a smokey burnout in front of the house just for the hell of
it..
Due to
my health problems it took all afternoon to get just this little job
done.. Sigh..
More to
come..
Rick
Draganowski
(it is good
to have friends)
Subject: Rustpuppy Test&Tune 93
Date: Wednesday, May 01, 2002 10:34 PM
Took
Rustpuppy out for a spin early this afternoon. The tank of 92 octane was just about empty so I couldn’t risk
any runs.. Got sidetracked helping a
neighbor look for the place the cows are escaping from the pasture above my
property.. I had been wondering about
the many cowpies littering my yard..
Later I
got a little nervous and emptied the 5 gallon lawnmower gas can into
Rustpuppy.. It was 87 octane unbranded
generic gasoline from the tiny country store just up the road so I didn’t
expect much..
It was
cloudy with a temperature of about 65 degrees but the humidity was going up and
I expected cold fog later. Rustpuppy
seemed perky with the 87 octane and I did a long joyful burnout through all of
first gear and half of second on the old road by my property.. I love this
crazy stuff..
At the
bottom of the old road I did a practice 0-60 run.. Time was fair at 4.88 seconds.. Up on Rustpuppy run I waited till traffic cleared and staged
for a southbound run.. Launch felt
good with just a bit more wheelspin than optimum (the high humidity factor) and
the run went straight and true for a time of 13.62@107.1
on the G-Tech.
This run
is the 141st since Goody was installed..
I have
removed the Pyrometer display system from Rustpuppy to send to Jim Acker but
substituted a new system I just got together.. Not fancy, and without the metal housing with the bare pc-boards
showing but it works good..
The
readings on the Pyrometer were:
1-1380
2-1290
3-1450
4-1330
5-1225
6-1290
7-1370
8-1325
Got
turned around on the first turn and waited for the traffic for a while. Then up on Rustpuppy run there was one
trailing slow moving SUV coming the other way and I waited impatiently on the
staging area till it passed..
This must
have made me nervous as after a poor launch with wheelspin through
all of
first gear I botched the 1-2 shift and had to abort the run.. I hate it when that happens.. Can you believe that I was so distracted
that I pulled the shift lever instead of pushing it? Duh...
So I
just called it a day and motored innocently home..
Tomorrow
I will be taking the Suburban in for
the rear axle rebuild job which will take place while I am fooling
around with the surgery thing..
More to
come..
Rick
Draganowski
(pulled
instead of pushing.. I can’t believe
it.. Duhh again..)
Subject: Rustpuppy Test&Tune 94
Date: Monday, May 20, 2002 5:25 PM
Two
weeks have passed since my neck surgery and I am still not supposed to
drive.. But, I have been driving for a little over a
week.. I been a bad boy.. I figure as long as I am careful and do
nothing that might
cause
problems with the healing I can get away with it.. Since I am in such a rural location the need for head turning is
minimized and I am using a hand held mirror on the occaisions that it is still
necessary..
Since I
have had a Pyrometer system set up to monitor the inlet temperature
This
definitely indicates a need for a cool air induction system of some kind.. I am planning on running a 4 inch diameter
connection between the cowl area on the passenger’s side and the air
cleaner.. This, along with the header
dump system are going to be the first serious changes to Rustpuppy as soon as I
recover enough to make it possible..
Due to
the neck surgery I managed to run a complete tank of gas through Rustpuppy with
no racing or even silly behaviour of any kind.. I drove her as if I were a law abiding and careful grandmother
with kids in the car.. Rustpuppy
rewarded me with the all time best milage (since the installation of Goody)
ever of 12.37 mpg.. Now this is short
trips (less than 15 miles) only so I bet at a steady speed on the highway she
could get 14mpg.. Amazing, since I am
used to between 8 and 10mpg...
More to
come..
Rick
Draganowski
Subject: Rustpuppy
Test&Tune 95
Date: Monday, May 27, 2002 1:35 PM
The
weather has be fair and windy for about a month and something is generating
serious pollen so my hay fever has been miserable. (coughing keeping me up at night) I decided to put up with the side effects of taking Benadryl so
I could get some sleep..
As usual
that damn stuff made me depressed and stupid like it always does..
Yesterday
even though it was still sunny the wind had died, temperature dropped, and I
could see the oncoming fog bank offshore headed in..
I was
out in Rustpuppy just taking an innocent little drive and noticed that there
was no traffic and no wind on Rustpuppy run.. Hmmm.. What to do?
You
guessed it.. I planned on letting
the TH350 shift itself so I could keep both hands on the wheel.. Staged for a southbound run on the best spot
of traction.. The launch was good with
just a bit of wheelspin.. The shifts
came up fast, 1-2 at 5400rpm and 2-3 at 4800 rpm so most of the quarter was in
3rd gear.. G-Tech time
was not bad for an autoshift run at 13.83@105 .
There
were no issues with my neck at all as I have good upper body strength and can
handle the .8 g acceleration easily..
With my confidence increasing I turned around on the short turnaround and
set up for a shifted run on the northbound good asphalt..
Launch
was not as good as the southbound run with more wheelspin and a bit of jog to
the left but everything fell into place for the reasonable time of 13.63@106.7 on the G-Tech.
I
expected the times to be slow due to the full tank of summer 92 octane and
the
highly restrictive cheapo 10” x 2” air cleaner I had installed
temporarily.. I am butchering up the old
77 truck air cleaner for a 4” cold air induction system.. I don’t know how Edelbrock can call this
pos air cleaner “Pro Flo”.. See
picture..
The
richer mixture from the inlet restriction caused the pyrometer readings to be
lower than normal by a small amount..
1-1309
2-1274
3-1394
4-1351
5-1202
6-1334
7-1289
8- used for
underhood temp - 148 degrees
One
thing in my defense (as I am sure to be yelled at for stupid behavior) is that
after all of my past orthopedic operations I have healed about twice as fast as
“normal” patients. This even caused
problems with my shoulder separation as they left the pin in for six weeks
which caused erosion of the bones and the doctor said that it should have come
out after only 3 weeks as I was totally healed by then.. So the 3 weeks since the operation is the
equivalent of 6 weeks recovery of a “normal” person and there was no risk in a
little careful racing.. (I suspect
it is my Viking genes which cause the fast healing, and the fact I am used to being beat up from my young days in
Chicago..)
Rick
Draganowski
(and the
racing helped with my depression, a lot..)
Subject: Rustpuppy Test&Tune 96
Date: Tuesday, June 04, 2002 2:53 PM
My shop
is orderly enough for me to be productive, at least in the front third.. (but I still can’t find anything) So I went ahead with the cold air induction
system for Rustpuppy.
I
calculated that 4 inch exhaust tubing would give enough flow and for sentiment
sake I wanted to stay with the stock truck air cleaner that came from my old
white truck when I transplanted the Target Master into Rustpuppy back in 1993..
My 14”
chopsaw is dwarfed by the 5 foot length of neat aluminized 14 gauge 4” exhaust
tubing I ordered in from NAPA.. That
stuff is not cheap at 6 bux per foot..
(See t&t96-1.jpg)
T&t96-2.jpg
shows the air cleaner and the snorkel that I plan on somehow attaching to
it.. The smaller practice pipe gives a
hint as to how..
After
carefully cutting the snorkel into two pieces I chucked one up in the lathe to
see how straight a cut I could make with the chopsaw using two passes.. (too big for single cut) It came out within 1/16” or so which is
fine.. (See t&t96-3.jpg)
Then it
was time to cut the part for the tapered end in half lengthwise with a metal
cutting abrasive disk on my trusty ol’
wormdrive.. (see t&t96-4.jpg,
t&t96-5.jpg and t&t96-6.jpg)
It was a pain
getting a straight cut and I plan on making future lengthwise cuts like this
while the pieces are still on the main tube to provide a stable location for
the foot of the saw.
Then
after clamping and tack welding the taper bits to the round part you can beging
to see where I am going with the project.. (see t&t96-7.jpg, t&t96-8.jpg, and t&t96-9.jpg)
I am not
up to speed on working and was tired at this point and called it a day..
More to
come, soon...
Rick
Draganowski
Subject: Rustpuppy Test&Tune 97
Date: Wednesday, June 05, 2002 3:55 AM
I welded
up the main part of the snorkel and then considered the flat sheets needed for
the triangular openings.. (see
t&t97-1.jpg)
After
learning my lesson on making the lengthwise cuts first I cut a couple of curved
pieces destined for flattening. (see
t&t97-2.jpg and t&t97-3.jpg)
Next you
can see “Draganowski’s Chunk-O-Steel” which I use as an anvil. It is a 3”x5”x11” block of steel in a nice wood case.. Heavy.. Getting out
the 2 ½ lb ball peen hammer I soon made flat ones out of curved ones.. See t&t97-4.jpg t&t97-5.jpg and
t&t97-6.jpg)
Strangely enough my shoulder has been hurting ever
since.. Not cut out for the heavy
work I guess..
Later that
evening (this was last Sunday) I was washing dishes and noticed
I
motored Rustpuppy down the old road in roaring fits and starts like a lunatic
trying to warm up the tranny fluid and get past the cold bog..
Then it was
time to stage on the southbound good patch of asphalt.. A scruffy looking old hitchhiker was
walking south on the Run just at that time.
And when I stopped to stage he thought I was stopping for him.
Poor
devil.. Then it was launch time but
there was just a trace of bog. Goody
was pulling pretty good with the 92 octane summer gas.. G-Tech Time was 13.57@107.4 .
I made a
quick turnaround at the first place and took off for the northbound staging
area.. Rustpuppy was perky with the 84
lbs off of the front, the 30 lbs of jack out of the back and with 90 lbs of
gasoline missing from the tank..
Started
picking up just a bit of wheelspin on the northbound launch but everything went
well for the time of 13.52@106.8 on the
G-Tech.. This is the 145th
run since Goody was installed..
Looking
forward to the improvements of the cold air induction and the exhaust cutouts
coming soon..
Rick
Draganowski
(racing is
good)
Subject: Rustpuppy Test&Tune 98
Date: Wednesday, June 05, 2002 6:10 PM
Had a
bad night and feel poorly today but still managed to get a little done this
afternoon.
After
hammering the curved pieces flat I cut one of them in half diagonally and
ground and trimmed till I got them to fit the triangular openings in the
snorkel..
Then
after clamping in place, tack welding, removing the clamps, and finish welding
I had both sides covered.. You
know, it is amazing how you can always find the hole in your welding glove when
you are handling hot metal.. Ouch!
See
t&t98-1.jpg through t&t98-6.jpg..
Calling
it a day at this point I went out in the Suburban to take my daily trip up the
hill.. On the way home I decided to see
how the ol’ Suburban would respond to some power braking. Too cool.. Lit up them big truck tires and the air was filled with the
sweet smell of burning tires.. See
t&T98-7.jpg Hoo haa!
More to
come..
Rick
Draganowski
Subject: Rustpuppy Test&Tune 99
Date: Sunday, June 09, 2002 12:05 AM
The
weather has been taking a sudden wintry turn with colder temps, cold showers,
cold wind, and nasty lower barometric pressure.. I been creaking and hurting and feeling low and depressed and
sorry for myself.. Took refuge in
Pizza Thursday and Friday night but it only provides temporary relief..
I
continued cutting cold steel and making lots of sparks in my shop working on
the cold air induction system for Rustpuppy.. I have the outlet end of the snorkel mostly done so I started
on the inlet end that attaches to the hole I am going to cut in the firewall
into the cowl airbox.. Since the inlet side cannot have any
discontinuities (steps or edges) it must be artfully designed and butt welded
(not the easy lap welding I done on the outlet flange) in a precision way..
Despite
feeling low I made good progress today..
Cutting, and grinding, and tack welding, and finish welding it came
together better than I expected..
See t&t99-1.jpg through t&t99-9.jpg..
I have the
Suburban all gassed up and ready for a roadtrip tomorrow to Medford.. Going to stay overnight and see my neck
docter Monday morning for the 5 week checkup on progress of my surgery.. I believe it is doing just fine so
far.. We will see..
I took Rustpuppy
the 7 ½ miles to the first little country store in Nesika beach to pick up some
chicken for a more healthful dinner and one that would let me get a good
night’s sleep..
On the
way there I noticed that there was no traffic,
the wind had slowed and was blowing directly down Rustpuppy Run.. And the showers had not wet the road down
there yet.. Hmmm... What should I do.. Yes.
Staging
for a southbound run and taking my time I got off a perfect launch and Goody
seemed to be pulling just fine for summer 92 octane gas.. The G-Tech time was good at 13.51@107.4 .
I had the Pyrometer system in Rustpuppy and jotted down the readings.
1-1259
2-1189
3-1323
4-1223
5-1186
6-1276
7-1229
8-1233
The new
Pyrometer software stores the highest reading in the numeric readout so the
exact readings can be recorded.. Much
better than interpreting the bar chart telltales.
You can
see the high octane summer gasoline burns much cooler and the pyrometer
readings are way down..
More to
come..
Rick
Draganowski
Subject: Rustpuppy Test&Tune 100
Date: Saturday, June 15, 2002 1:58 PM
Slowly got
back into the cold air induction snorkel project last week.. You can see the
location of all the spark making in t&t100-1.jpg...
I just wish I had
the dough to finish the inside and get the entrance ramp done.. Oh well. It will happen in time..
Back on
the project. I used the other
flattened hunk of tubing for the sides of the intake end of the snorkel system
that will be welded to the firewall..
See the clamping, spot welding, and finish welding in t&t100-2.jpg
through t&t100-7.jpg.. Getting routine
but it looks like my welding technique is degrading.. Having some problems seeing what is going on when under the
hood..
Then it was
time to cut off the excess material with the abrasive disc in the wormdrive
saw.. What a noise and cloud of
stinking dust that makes.. Cutting
through the welds was tough and after two cuts my saw disc had shrunk to
practically nothing.. See t&t100-8.jpg
through t&t100-10.jpg..
Now for
something completely different.. All
of the racing and fooling around with Rustpuppy had just about finished the
tank of 92 octane Texaco gas and I decided to test the good smelling generic 87
octane from the little country store in Nesika Beach about 7 miles from
here.. I got some for the mower last
week and it smelled like real gasoline instead of the normal modern additive
filled junk..
I had
them put just 5 gallons for the test.
The tank probably had about 3 or 4 gallons of the 92 octane left..
Then on
the way home I noticed that the road was dry..
The wind had died to nothing..
There was a lot of traffic but I started getting ideas.. I
pulled
off the highway at the second turnaround on the south end of Rustpuppy
Run.. (the one the state police staked
out a few months back)
Then I
waited for a break in the traffic..
It was about 4pm on Friday afternoon.. Finally it cleared up and I took off for the staging area on
the south end of the run..
It was a
good launch and Goody seemed to be pulling well.. Everything went OK and Rustpuppy was tracking arrow straight in
the center of her lane..
The
G-Tech showed a time of 13.54@107.5.. Hmmm..
About exactly the same as the last tests with the 92 octane.. Sigh..
I guess the good smell was not a good indication..
On the
way home I stopped at the top of the hill and Goody ran over a bit after I
switched the ignition off.. Looks
like I better stick to the 92 octane since that never happens when I use it.
I copied
down the max readings on the Pyrometer made during the run..
1-1352
2-1261
3-1430
4-1309
5-1240
6-1329
7-1334
8-1308
About
the same as the last readings using the 92 octane gas.. Same times, same temps.. With the good gas last February the
readings were over 100 degrees higher and the times were about a tenth quicker..
More to
come..
Subject: Rustpuppy Test&Tune 101
Date: Saturday, June 15, 2002 10:47 PM
Next
chapter of the never ending saga of the Rustpuppy Cold Air Induction
Flange-Up...
I used
the neat (and very cheap) Chinese Harbor Freight air saw to finish the trimming
on the inlet flange..
(t&t101-1.jpg and t&t101-2.jpg)
Then it was grinding and sanding till the parts were
acceptable.. Lotsa sparks..
The
flanges are side by side in t&t101-3.jpg and you can see into the funnels
in t&t101-4.jpg(outlet) and t&t101-5.jpg(inlet).. The inlet with a nice smooth transition
and the outlet with the step..
Then I
took the parts outside and puzzled over the actual installation in
Rustpuppy.. My original plan was to
have the inlet snorkel flange in the plenum in the firewall above the aluminum
door in the hole the heater/air conditioner used to live in.. And then the outlet snorkel flange in the
air cleaner pointing forward about 30 degrees to the right front corner of the
engine compartment..
After
holding the parts in place it became obvious that my original design was a
stinker.. The hose would have to make
a sharp 120 degree turn and the results would be less than ideal. And the appearance would be repugnant..
So after
sitting in front of Rustpuppy and thinking and looking I came up with plan
number 2.. Here it is..
First
mount the inlet flange under the right headlight next to where the license
plate is bolted.. Plenty of room and
it can lurk in there with the bumper replaced and no one would suspect.
See
test&tune101-6.jpg...
Then cut
a big hole for the hose in the right inner fender panel and lead the hose up to
the outlet flange welded to the air cleaner..
Test&tune101-7.jpg shows the discarded narrow nasty location I was
considering for the inlet flange..
Test&tune101-8.jpg shows the cool location for a nice 4 inch hose to
snake through the inner fender panel..
Wish me
luck..
More to
come..
Rick
Draganowski
Subject: Rustpuppy Test&Tune 102
Date: Sunday, June 16, 2002 10:19 PM
The day
started innocently enough.. I went down
to the bottom of the other side of the hill in the Suburban to take a picture
of the improved road signs that our County road department fixed on my
request.. I wanted to send a thank you
e-mail for their quick and professional work.. Then when I got home I parked the Suburban at the top of the
lawn by Junkyard Dawg so I could turn Rustpuppy around and get her up on the
ramps to examine the area in the inner fender panel where the hole has to go..
Then I
remembered that I needed to take another roadsign picture of the end of the
County road where the signs there have deteriorated as well.. Might as well try to get them fixed
too.. So I took Rustpuppy to get her
warmed up and turned around to go up the ramps.. Well I decided to go all the way to the other side of the hill
(2 miles) to get Goody warmed up properly and when I went to turn around at the
bottom of the hill I noticed that the weather was perfect.. About 65 degrees and dry and sunny.. No wind.. Hmmm... Maybe just
one more test Run?
Lots of
traffic since it was about 11am and everyone was going somewhere for Father’s
Day.. I hung around at the north end
of Rustpuppy Run for a while and the traffic was non-stop.. Sigh..
I took
off down to the south turnaround with no racing due to the traffic.. I planned
on just going home.. When I got to
the northbound launch area the traffic had miraculously disappeared.. Great.
Plenty of time for a clean stage on the prime bit of asphalt for a
northbound run..
I could
tell with the launch that this run was going to be special.. Just a hint of wheelspin and lotsa G
forces.. Good traction for the 1-2
shift and just another push in the back..
I could tell by the way that Goody was winding that this was going to be
a good one..
And it
was.. The G-Tech was blinking 13.37@108.8 for the very best time Rustpuppy has
ever had. Hoo haa!
I was so
worked up about it that I kept Goody running and motored home to get the video cam
to take pictures of the event..
During the fooling around I got quite a snootful of exhaust fumes.. But they smelled great with the good 87
octane gas from the country store..
See the G-Tech readout pictures at t&t102-1.jpg and
t&t102-2.jpg..
I jotted
down the Pyrometer readings..
1-1339
2-1263
3-1435
4-1325
5-1247
6-1338
7-1327
8-1293
Still
stoked about the good G-Tech time and a bit wonky from the exhaust fumes I set
up the stamped steel ramps to drive Rustpuppy’s front wheels up on.. Something went wrong as the ramps slid in
the gravel drive (I am used to using them on grass) and when they caught it was
impossible to slow down and stop in the shallow recess in the top of the ramps.
So I
drove Rustpuppy off the back of the damn ramps and she came down with a shattering
crash. Oh no! I’ve wrecked poor Rustpuppy! But the bulk of the impact was on the
right front fender behind the wheel..
It was in poor condition to
start with.. See smashup picture
t&t102-3.jpg..
Where the bottom
goes up at an angle is supposed to be straight.. Oh well.. On to some
work..
Today I
addressed the issue of squishing the end of the outlet funnel to fit (somewhat)
to the air cleaner base.. You can
see from t&t102-4.jpg that it starts way too big..
Then it
was a matter of squishing it in the Kurt AngLock vise on the Bridgeport and
clamping and prying with the big damn screwdriver to slowly shrink the height
of the end of the funnel.. See
t&t102-5,jpg through t&t102-8.jpg for snapshots of the process..
It ended today with about a half inch to go but looking
much more like it may fit someday.. See
t&t102-9.jpg..
By this
time it was late.. About 4:30 or so and
I couldn’t hear any traffic.. Weather
had changed a bit with some clouds and increased humidity.. I had the air cleaner completely off
Rustpuppy and got an idea for another test..
Yeah, right.. Idea..
Remembering
to remove and store for safe-keeping the gasket on the Q-Jet airhorn I piled
into Rustpuppy for some more racing..
(last time I ran Rustpuppy without an air cleaner I forgot and left the
gasket and never saw it again..) I
also had found that I had neglected the air pressure in the front BFG’s and it
was only about 22 lbs.. I aired them up
to 35 psi..
No
traffic so I had plenty of time to stage on the southbound Run.. The
launch
was disappointing with too much wheelspin (about half way through first) and I
didn’t expect much for the time.. I
was right.. The G-Tech time was only 13.48@107.6.
But the added air in the front tires made the handling and tracking feel
even better than before.. I like it..
I jotted
down the Pyrometer readings..
1-1334
2-1218
3-1432
4-1324
5-1220
6-1287
7-1352
8-1264
Then it
was on to the second turnaround and back up to the northbound staging
area.. I tried to get exactly where
the great time was this morning.. But
the evening mist from the Pacific was creeping in and the traction I found this
morning was gone.. The launch was
soft with wheelspin almost all the way through first and then a long hit of it
in second.. Sigh.. Not much to expect.. The G-Tech time was 13.52@107.1
.
And the Pyrometer
readings were:
1-1352
2-1231
3-1421
4-1288
5-1188
6-1262
7-1346
8-1273
It seems
like the fuel distribution from the Q-Jet is disturbed by running without an
air cleaner that has the curved base like the old stock truck air cleaner I am
fooling with..
More to
come..
Rick
Draganowski
(Smash-um
and crash-um.. Idiot..)