Subject: Cynthia’s oil pump
Date: Friday,
July 18, 2003 9:44 AM
Since I had
it out and lying around I decided to open it up and share what I found. The oil pump gets the
garbage and metal from the sump directly and
Looked
even worse than I expected with serious wear on the end plates and deep
scratches on the rotors and strange looking combination ding and scratch on the
walls of the pump that meet the rotors.
Here are
the three best pictures. The
rotors are underexposed to emphasize the scratches in the gear flanks..
(cyn-pu-1.jpg, cyn-pu-2.jpg, cyn-pu-3.jpg)
Nasty
things were happening in there.
More to
come.
Rick
Draganowski
Subject: Rustpuppy Test&Tune 167
Date: Sunday,
July 20, 2003 7:43 AM
Due to
health issues all of my projects have been stalled for a while. I will explain more about
them tomorrow.
Anyway,
I managed to get Rustpuppy down from the jackstands where she has been for that
last couple months. When
she was up I spent some time underneath inspecting everything.
I think
I found part of the reason that the slip yoke on Rustpuppy is showing 1.5”.
(which seems like too much)
The
slotted hole for transmission mount stud
on the crossmember is long and there is room for a lot of
adjustment. I decided to take some
action on this issue.
First
after loosening the transmission mount stud I pried on the motor mounts to see
if the insides would change location. I got the motor to move back about 1/8” that way but
it still could move another 3/8” if I could pull on it hard enough. I spent a few weeks figuring out
a method of generating a 2000 lb (or more) force pulling the motor back to
assist the prying. When
Goody is in her proper location I can tighten the transmission mount stud and
that should stabilize the location. Naturally after installing the kludge it
involved jacking Rustpuppy back up..
I am
hoping to get the slip yoke in a more normal configuration.
Yesterday
I finished putting together the system to generate the ton or more of
force. See
t&167-2.jpg and
t&167-3.jpg.
I left
it pulling all night to see if the rubber in the mounts would flow and adapt..
In the
process of figuring out how to apply that large force without
Also I
was concerned that the slip yoke being out of place may have damaged the
tailshaft bearing. I set up
a dial indicator on the end of the yoke at the u-joint and measured the deflection
with a 70 lb force in each direction. Since I have a spare tailshaft housing and slip
yoke I have all the necessary dimensions to work backwards from that movement
to the actual clearance in the bearing.
(which is only 0.910 inches wide BTW)
It
worked out to 0.003 which is what I would have specified for a sleeve bearing
that size in that application.
So there has been no damage at all and another bit of paranoia is put to
rest. I
need to repeat this procedure on the Suburban now. But it will have to wait till I am better.
Much
more to come.
Subject: Non Nova Rick’s heart attack
Date: Monday,
July 21, 2003 9:19 AM
The
Thursday before G03 (the 10th of this month) at 5AM I had a serious
heart attack. I wasted
time at first since the initial focus of the heart pain was under my left
shoulderblade only 2 inches from where I ruptured the disk.
I have
had these before but this was a very bad one. Then the pain intensified quickly boring through to my
left chest and down my left arm. I
had the vise like sensation on my chest and couldn’t breathe. I have worked in cardiac
care so I knew exactly what was happening and what to do.
I knew
how much oxygen is stored in my tissues so I knew how much time I had. My vision was blacking out before
I could get to my heart medicine so I did the high G exercise I was taught back
when I flew aerobatics. I
got to the medication and did the other things possible at home for treatment
and pulled through this one.
It was a
big one and it did a lot of damage to my heart muscle (left ventricle) I went in Monday to Dr. Williams and
reported what happened. The
aftermath symptoms were so severe that I suspected electrical path block. I insisted on an EKG so I could
see my strip. It indicated
electrical path block exactly where I expected and that may cause me other
problems in the future.
(reentrant tachycardia)..
But the
strip also showed that enough of my big heart was functioning normally that I
was in no danger of a repeat performance.
At least not in the immediate future.
Dr. Williams
wanted me to go to the hospital for a few days for observation but I convinced
him that at this point they couldn’t do any more for me than I could do at
home. Since the damage
is so large it is going to take a long time to recover from this one so I am
going to be out of it for some time.
I didn’t
want to piss on the G03 celebration so I kept my mouth shut about this until
now. There are a lot
of physical and mental issues in the recovery phase of a serious heart attack
so I may not seem normal in my posting. I am sorry if I get on someone’s nerves.
I will
be in bed with the laptop a lot so I will be in constant touch. For the most part my attitude is
good and I promise to care for myself properly.
Thanks
for listening.
Subject: Working on Rustpuppy
Date: Monday,
July 21, 2003 4:24 PM
You guys
and Ladies know that I can’t lie to the list. I got so sick of lying in bed this afternoon that I
went out and worked for an hour. I
did have to go out for water and food since I have no running water or
refrigerator where I live now. But
instead of just returning to bed I went out to my shop.
Most of
the time was spent in my shop sitting down and finishing a project I am doing
for a sick woman who needs help.
But I
did get under the hood on Rustpuppy. The tension rig on the driver’s side had bottomed and one
of the chain loops needed shortening. I spent about 20 minutes on that.
I was
tempted to crawl under Rustpuppy with the crowbar and do a little prying but I
knew you all would give me hell if I did that. So I am back in bed taking it easy. I did manage to work up a
little sweat and just that makes me feel better mentally.
I am
such a nut.
Subject: Explanation of Old
Draganowski’s heart stuff
Date: Tuesday,
July 22, 2003 5:56 AM
(Editor’s
Note, A few of the list members
questioned my sanity for taking care of my heart attack by myself. Here is my response..)
You
don’t understand my status regarding this. I worked in research on the first computer monitoring
of cardiac intensive care patients (using mainframe computers) and this stuff
was just part of my daily work.
I worked
with Dr. Budkin’s group at Miami Heart Institute. It was one of the research centers that developed
the cardiac catheterization test. I probably watched a hundred people die of
heart problems during this part of my career. I know exactly how tough most
people are and the amount of damage and time it takes to kill. I would scrub and be in the operating
theatre during the catheterization test development. Since our patients were all in the last stages of terminal
heart disease our mortality rate was about 25-30% during the surgery. And I
helped in the writing of the first successful EKG analysis teaching
program. So there are no
mysteries in this subject for me.
When I
got sick with my heart issue back in 1992 I dug out my books and built a 12
lead EKG machine so I could monitor and treat myself. My cardiologist was an idiot who damn near killed me
with too large doses of the wrong drugs. I still have liver damage from his screwup. (he left town, and I hear he is out of
Medicine now due to malpractice issues)
I have had 5 heart attacks before and managed all of them This one just
I must
be able to manage it myself, there is no real alternative for me. With proper diet, stress control and a
relatively new medication I have had it under control for about 5 years
now. But this episode took
me by surprise.. I am not
doing this for the fun of it.
Subject: Rustpuppy Test&Tune 168
Date: Thursday,
July 24, 2003 8:59 AM
I have
reached the point in my recovery that it is essential that I get a
I felt
good so went back out to remove the chains and clamps that were putting the pressure
on the motor mounts.
Taking my time found that I
could comfortably lean on the fenders and remove the chains, clamps, and wire
cables. Next it was a matter
of carefully fitting the expanded snorkel tube to restore Rustpuppy’s cold air
intake system. I had
spent 5 hours doing about a 45 minutes worth of work so you can see I am not
overworking myself.
Then I
removed the wheel chocks and checked the oil. Do you have an idea where this is heading?
It has
been over two months of misery since the last time I started Goody
She
sounded so sweet and beautiful that it brought tears to my eyes. And
“go like
hell” for a bit..
The
feeling of the g-forces pushing me against
According
to my time sense it was about 1/3 of a second. And sometimes a bit longer due to higher vacuum stored
in the diaphram housing.
I think for optimum usage of the Drag Radials this delay (which made it
possible to do pretty well on street tires) is not needed and is slowing
Rustpuppy down. Just disconnecting
the vacuum hose and plugging it will disable this function and allow instant
response from the secondaries. Will be fooling with that later today.
It
looked like I was out of gas so there would be no more fun till I go to town
and get 5 gallons of 92 octane for the Pup.
Driving
slowly back home (with just two exceptions) I decided to park Rustpuppy on the
crest of the hill in front of my shop so the front wheels are elevated enough
for me the crawl under and see how much good all of the pulling on the motor
mounts did.
After doing that and getting the measurement I was disappointed to find
that there was no apparent change in the dimension of the exposed slip
joint. Damn, a lot of
work for nothing. I noticed when I
was under prying earlier that there seemed to be metal spacers embedded in the
rubber to prevent much fore-and-aft movement. So much for that theory. Poop.
Yesterday
I had to go to town for groceries and a business meeting. Got
Quite a slant there. I plan on vacuuming her out and
All this
time the temporary spot welds that held the right side cutout in place worked
just fine and I couldn’t even hear an exhaust leak.
In a day
or two I will put Rustpuppy back up on the jackstands on the other side and get
going on the left cutout installation.
More to
come.
Subject: Rustpuppy Test&Tune 169
Date: Thursday,
July 24, 2003 4:04 PM
Rats.
Felt good this morning. Went out and planned on getting on the “clean up
So I
spent quite a bit of my time re-arranging my junk so I could park the Pup in a
more reasonable work location. Finally finished the organization (takes a long
time since I am so far behind in everything) and was just messing around with
some aluminum flashing for a new dash cover for Rustpuppy when I messed my self
up for the rest of the day.
I have
to be so damn careful.
What happened is this. I was sitting in my chair trying to mark a cut
After a
few seconds of this position I was in trouble.
By
bending forward that much you increase the abdominal pressure by a considerable
amount. This pushes up
against the heart pressing it against the breastbone. In addition the heart is inverted and not
suspended in it’s normal location so it’s weight is pressing against the
breastbone.
This
would not be a problem for normal healthy folk. But old idiot Draganowski was pressing hard right on
the spot on the front of his heart that has the damage and is trying to
heal. Really pissed my
heart off and it let me know about it.
At that
point it was time to go back to bed and no further work was possible today.
I have
to be so careful..
Attached
is a picture of Rustpuppy in her new, more reasonable work location.
More to
come.
Rick
Draganowski
(dumber than
a bag of dirt)
Subject: Rustpuppy Test&Tune 170
Date: Sunday,
July 27, 2003 6:56 PM
Been feeling
down with the effects of the healing process on my heart but managed to spend
some time on ol’ Rustpuppy.
Housekeeping
first. Vacuuming and cleaning
windows, Ospho on the floor of the trunk followed by a nice thick coat of black
acrylic brush-on paint.
Got to
the tech stuff finally.
(spent days on the few hours work of the
I had tested the time
I tested
the old pre-smog one on Rustpuppy and it was only 0.2 or 0.3 seconds of
delay. Exactly what my
subjective time sense came up with back in Test&Tune 168.. It had to go..
First I
had planned on removing the vacuum hose and plugging it.. Ha!
Fat
chance. Not only is it short
but it is hidden behind the fuel line.
And it is the original hose that has been on there since 1975.. It seemed to be made of solid
hard rubber and permanently molded to the ports.. Rats.
Everything
bent except what needed to be..
Sigh..
Then I
just sat down for a while and looked at the simple little mechanism that had so
far defeated me.. A
bit of thinking came up with this idea.
Just drill a 1/16” hole in the vacuum side of the diaphragm and that
would bleed off the forces needed to move it against the spring to clamp the
air doors.. Hoo Haa! Sounds much
easier. And the beauty of this
plan is that it is reversible by just plugging the tiny hole..
See t&170-2.jpg and notice the wee little hole in the vacuum
pot..
Some
Putting
everything together in the engine compartment I took a snapshot..
Then the
5 gallons of 92 octane went in..
Then it
was time to go up the hill onto the new asphalt area of my old road for some
testing..
By this
time I was feeling pretty weak so I didn’t spend much time fooling around with
the testing.. Goody never
got properly warmed up.. But
even though she still had a bit of a cold bog seemed more instantly responsive
to the throttle.. Good show..
Another
thing I tried is to figure out the braked stall on Rustpuppy now..
Got on
the brakes hard and slowly increased the throttle opening. Rustpuppy hunched up and creaked like
she does when I do this unnatural thing.. At 2450 she started pushing the front
disks and I stood on the brakes as hard as I could (worrying that I may bend
the pedal) and got her stopped. Rpm kept building and at a hair above
2550 the Drag Radials started spinning. Slow at first with a swooshing noise. Then instantly building to a
scream with the cloud of tire smoke that happens when they lose traction big..
What is
the relationship between braked stall and launch stall? I forget what I read about
it..
Time to
go home and rest.
More to
come..
Rick
Draganowski
Subject: Rustpuppy Test&Tune 171
Date: Tuesday,
July 29, 2003 4:56 PM
A little
depressed this morning..
Found out that my coolest and best
I took
Rustpuppy for a ride to cheer me up. I really should have her jacked
Warm day
for up here at 80 degrees with little wind.. I motored down to the end of the old road to the
spot where I do the 0-60 runs and tried one. It felt great to be going like hell again.. Time was OK at 4.77 seconds.
Then I
decided to scout out Rustpuppy Run.. Conditions were perfect for some racing.
But.
There
seemed to be an endless stream of motor homes and tourists going in
Something strange happened at speed.. I noticed that the lift effects on Rustpuppy’s
nose above 110mph had pulled up a
rusty piece of her hood.. See t&171-1.jpg
On the
way home at the top of the hill where I fool around on the new asphalt I
decided to do a G-Tech G-Force reading..
Goody and the transmission were at the top of their normal operating temp
and I was hoping for a better stall rpm..
The
launch seemed less abrupt than usual and I started wondering what was
With the
street tires when they started spinning they stopped pulling almost
completely.. It
is going to take some getting used to these racing tires..
Parked
Rustpuppy with hot tires on my hot gravel drive and did some work in my
shop. Then I moved Rustpuppy
a little and noticed this phenomena..
Them tires is sticky..
See t&171-2.jpg and t&171-3.jpg..
It was
fun but I am going to quit fooling
around and get Rustpuppy jacked up to finish the cutout installation..
By the
way, the pig’s ear spot
welds I made on the passenger side cutouts held up fine to all this abuse..
More to
come..
Subject: Rustpuppy Test&Tune 172
Date: Thursday,
July 31, 2003 11:42 AM
Made my
mind up yesterday that I was jacking Rustpuppy up and putting her on jackstands
to get the driver’s side cutout installed.
Then
early this morning something started bothering me. Looked out about 5 am and noticed that the
condensation levels were way down and it seemed dryer than it has in days. (we have been having foggy
mornings)
Then
later at about 8am a little idea crept into my demented brain.. I could hear the
traffic below on highway 101 and it seemed really light..
Hmm..
By 8:15
I was sitting in Rustpuppy warming up Goody.. The sun had been
I
motored quietly (in second gear) down to the end of the old road.. Staged for a 0-60 practice run.. A little bit of tire spin
from the Drag Radials (but not much) and a nice time of 4.69 seconds..
Then it was up to Rustpuppy Run. Sat at the entrance waiting for a clear
southbound
staging area and tried to settle my nerves. When I hit the go button on the G-Tech I knocked it out
of level. And by the time I
got that straightened out a car appeared oncoming around the bend about a mile
and a half south of where I was..
Rats..
Motored down to the first turnaround and waited for clear
traffic. Got a
clear. And it
was time to go. Launch
seemed soft as the traction at the
was. Time on
the G-Tech was 13.40@109.7.. I like it.
Got skunked
on another try at a proper southbound run by the carefully timed and
inconvenient traffic..
So wound up with another northbound run..
Tried
staging a little further up this time hoping for slightly better
As time
passed with me farting around waiting for breaks in the traffic flow the road
was getting dryer and better each minute..
Finally
got a chance at southbound run.. I was hoping for a little better time with
better traction. The launch
was a much harder hit and the run felt good.. I am having too much fun to be
legal..
The time was 13.34@107.7 on the
G-Tech.. I may have got off
the gas just a little bit early on the end of this run..
Final
run of the morning coming up..
I am so worked up I though my head would explode.. This time on a
northbound run I tried a new spot of asphalt that they had patched Rustpuppy
Run with about 2 years ago.. Never
launched on it before as it shortens the braking distance at the end.
This launch
felt the best and the run was great.. Goody was running as
Time to
motor home like a good citizen.
It was all over by 8:45.. Half
Will be
going out in a few minutes and put a temporary halt to this madness by putting
Rustpuppy up on the jackstands..
What a
wonderful morning I had..
p.s. Rustpuppy was running light with
nothing in the trunk, front bumper off, and only 5 gallons of gas in the
tank.. And I am considerably
lighter as well..
Subject: Rustpuppy Test&Tune 173
Date: Wednesday,
August 06, 2003 8:59 AM
No way
can the excitement of Test&Tune 172 be maintained.. Back to dull plodding auto
mechanics stuff..
Rustpuppy
got jacked up for the left cutout implant the day after the racing.. Since I am in recovery from
that damn heart attack I get tired so quickly that it took all the next day
just for this little job..
Pathetic..
(See t&173-1.jpg and t&173-2.jpg)
My first task is getting the rusted and jammed on rear brake
drum off.. I had ground on
the inner edge of the drum openings and the ridge on the centering spigot on
the axles the last time the drums were off (had a hell of a time with them
then) but I didn’t want to mess up the centering of the drum so I took a
minimum amount of metal off..
It wasn’t enough.. A little bit of corrosion plus the slight
I
finally hit on the procedure of pulling on the drum. I would pull the axle out to the C-Clip and hit the end of the axle back toward
the center pin and depend on the inertia of the drum to do the pulling. Worked good but it took
quite a while as only a tiny amount of movement was possible with each impact.
Finally
it was off!.. (see
t&173-4.jpg)
I was relieved that I didn’t have to fool with home made
pullers again.. (that shoot brake
drums at your stomach unexpectedly)
Whenever
I have the opportunity I check Rustpuppy’s brakes and verify that they are in
top condition.. Looks
damn good in there to me.. (see t&173-5.jpg)
Time to get serious about that clearance issue.. Out came the trusty die
and
until the clearance was
more than any rust could block.
I also applied a thin layer of chassis grease to the spigot and hole to
protect them from corrosion..
I don’t want to go through this again..
Then the weather changed for the worse.. Cold fronts, fog, light
drizzle,
I did
spend some time in the shop cleaning up. Then I used the vice grips to pull the
silly tin caps out of Rustpuppy’s phony acorn lug nuts. Then I chucked them in the lathe and
turned off the hollow ends to make them pretty.. (See t&173-9.jpg)
More to
come.
Subject: Rustpuppy Test&Tune 174
Date: Thursday,
August 14, 2003 9:16 AM
This
report is not as happy as most as I have found out (the hard way) about the
major down side of the new BFGoodrich Drag Radials.
They
have been tuning the rubber compound to maximize the traction at launch
Rustpuppy
has less than 200 miles on her Drag Radials and only ten quarter mile
runs. An
additional ten 0-60mph runs and about 8 or 10 burnouts. None lasting more than 2 seconds.
That has
used up about 50-60% of the tread they started with. Damn, this is going to get expensive..
See
pictures. (t&174-1.jpg,
t&174-2.jpg, and t&174-3.jpg)
(not
alone, you should see how the Mustang crowd is bitching)
Subject: Rustpuppy Test&Tune 175
Date: Monday,
August 18, 2003 11:40 AM
This
report is a mixed bag of subjects.
I figured
out a way to secure the exhaust pipe on the driver’s side so that cutting it
with the hacksaw would be safe for me. When I did the passenger side I ruptured a disk in my
back due to my carelessness.
It is 14 or 16 gauge stainless so I know it will require more than an
hour of sawing.
I pulled
it down as far as possible and clamped it to one of the jackstands
On the
subject of cutouts I have a theory as to why some motors with mild cams like
Goody like to have a longer pipe on the cutouts than straight out some short
distance behind the collectors. It is that the pressure wave generated by
reflection at the open end of the cutout interferes with the operation of the
pressure wave generated by the header pipes opening into the collector and
spoil the tuning. This
effect is strongly dependent on cam timing and rpm so it varies so much that it
cannot be predicted very well.
Rustpuppy’s cutout pipes extend 50 inches from the collector outlets and
the cutout opening reflections shouldn’t interfere. That is what I am hoping anyway. But the main reason they
are so long is to make it easy for an ol’ cripple to operate them without crawling
on the ground.
I got
sick of looking at the sorry wrinkled and deteriorated aluminized cardboard
dash pad on Rustpuppy and spent some time making a replacement out of wide
aluminum flashing. I
added the struts to prevent it from vibrating. (See t&175-2d.jpg and t&175-3d.jpg)
After
the cutouts have been tested (bet they will be loud) I have more plans for
Rustpuppy. Waiting in
the wings is another performance modification. I put the Victor Jr. intake manifold with the Edelbrock
special single-plane to Q-Jet adapter plus the modified for racing Q-Jet on
Cynthia to get dimensions and get a fuel line together for it. It is considerably taller than
the ordinary Performer manifold on Goody now but I am hoping to fit it under
the hood. (see t&175-4d.jpg)
A
curious phenomenon has been taking place during the last 180 quarter mile runs
ol’ Rustpuppy has made.
When I grab for second or third on the shifter I use a strong grip so
there is no chance of my hand slipping.
This habit combined with the small rotation of my lower arm due to the
straightening of my elbow has generated a tiny but powerful rotation clockwise
on the shift knob. Despite
the locknut being tight it has rotated one complete revolution plus almost
another 90 degrees. I have
been watching this and I thought I would share it with the list. (see t&175-5d.jpg)
Now we
get to the serious part of this report. As the list knows I cannot stop analyzing
problems once I start. I
think of them at odd times throughout each day until I am satisfied with the
solution. It must be from
part of my training or something.
Anyway I have been mentally picking at the “rip the tread off the Drag
Radials” phenomenon. There
were several bits of information about the problem that I had not properly
thought through.
One of
them being that I have the habit of visually inspecting the tires on
So the
conclusion is that almost all of the damage to the Drag Radials was done by the
single 0-60 run and the four quarter mile runs documented in Test&Tune 172..
Damn. They were all back to back with
no inspection of the tires so I had no idea it was happening. And I was launching on the
most abrasive parts of Rustpuppy Run that gave the best time with the street
tires so everything was set for the problem to appear.
We live
and learn.
I am
putting the street tires back on Rustpuppy and taking out the Q-Jet
modification and reserving the Drag Radials and the mod for track use
only. No more running them on the
street. This picture
shows the status of the street tires with 170 quarter mile runs and 5000
highway miles compared with the Drag Radials after four quarter mile runs and
about 140 highway miles. (see
t&175-6d.jpg)
I am probably
buying the Firestone Indy 500 tires (235/60-14) to replace the worn-out
BFGoodrich street tires.
More to
come.
Subject: Test&Tune 176
Date: Friday,
September 05, 2003 7:00 AM
Test&Tune
175 left off with the exhaust pipe on the driver’s side positioned for an easy
hacksaw cut. I promised myself that no matter how long it takes I will not hurt
myself doing the sawing.
I did
the cut and despite not having room to sit up during it still was in a
comfortable position.
I took my time and never did more than 10 minutes cutting at a time. It took a couple days as a result. Patience pays off. Results are in t&176-1.jpg.
No
problems this time as I really learned a lesson by hurting my back on the last
manual cut. I have the chopsaw in
a better and more permanent location.
Note the spark catcher.. It is set up for the second cut on the exhaust
stub
I am hoping for a better
fit on this side to cut down on the
Amazingly,
it fitted together perfectly and would stay in place by just being pushed
together.. Much
better. t&176-4a.jpg and
t&176-5a.jpg show the
miracle. I still worried
about it falling apart so I rigged some wire and clamps to hold the assembly
together. It shows up in
later pictures.
Next
morning I checked outside at 4am and found no wind for a change. So it was time to take a shot at spot
welding this side. I
needed some coffee and breakfast to get me going so it was shortly before 5am
that I was out wrestling with my heavy welder. Some near disasters as a wheel slipped off the ramp
and almost tipped the thing over.. Despite the temperature of about 50 degrees I
was sweating when I took this picture.
t&176-7c.jpg.
By this
time it was almost 6am and the sky was beginning to lighten. And the
I
promised myself to start much earlier the next try. Grinding down the initial pig’s ear welds showed
about 3 adequate spots under the garbage.
See t&176-9c.jpg.
Part of my welding was in still air so it wasn’t a total
waste of time. I left the
welder out next to Rustpuppy that night with everything in readiness. I even added a cardboard
and tarp wind screen to block the wind on the west and north sides of the work
area.
Tomorrow
is another day.
Subject: Rustpuppy Test&Tune 177
Date: Friday,
September 05, 2003 5:07 PM
In the
last report I made a pig’s ear out of the initial cutout welding due to
I got
breakfast and my coffee down and was out next to Rustpuppy at the pitch
Poop!
Falling
back on stubborn and stupid I rewelded yesterday’s work and managed one more
section before being forced to give up. But enough metal was on to secure the
pipes and prevent any separation.
The wire and clamp kludge came off. I was hopping mad and swore that I would beat
this problem or else..
Some of
the welds today were pretty good and plenty of metal was put down. The slight wind was just enough to make
them ugly.. See
pictures t&177-1.jpg, t&177-2.jpg, t&177-3.jpg, and
t&177-4.jpg..
It looks
like I may have to take drastic steps.
We will
see..
Rick
Draganowski
(damn wind)
Subject: Rustpuppy Test&Tune 178
Date: Saturday,
September 06, 2003 11:17 AM
So there
I was. Despite all of my
best efforts including getting up at the unholy hour of 3am the welds were not
finished. Like I said
before “drastic measures will be taken”.
I did my
best not to think about Rustpuppy the rest of the day but the issue kept
gnawing at my peace of mind.
I went to bed early that evening at about 7pm hoping to get a good
night’s sleep.
But.
Just
before 11pm I awoke filled with a terrible resolve. (after about 4 hours of
sleep) Some small rational part of
my mind protested my insane behavior but I was dressed and out the door to
Rustpuppy’s side by 11:15pm.. Basically the middle of my night.
Finally,
there was no wind. I was
tired and had some physical issues but pressed on regardless. Lights on and positioned
for the inside welding and gear in place I pulled myself under enough to see
and reach the side of the pipes closest to the center of the car.
The
welds started OK and despite being a bit sloppy were just fine for this
application. See
t&178-1.jpg for a partial indication of the beginning of this midnight
adventure.
It seemed to be going well.
But.
On the
other end of the cutout (toward the front) and the most difficult to
At first
I felt unusual heat on the right side of my neck up under the edge of the
helmet. Then my helmet
filled with smoke. Damn. I had set fire to myself.
So there
I was, with the cables to the welder across my stomach and chest and way under
the jacked up Rustpuppy with precious little room to maneuver and I was on fire.
My next
coherent memories were of me out from under the Pup beating my burning coat
into the dusty gravel of my driveway. Some automatic system in my brain must have kicked in
since I have no memory of how I got out from under and got the coat off before
getting any burns. The
fires (two of them) started in my right collar and was very close to my tender
neck. See t&178-3.jpg.
What had
happened is some large droplets of white hot molten metal from my blind
The
reason for my blindness and the trigger for this debacle was simple. I was not dazzled by the
arc. The stupid knob that
sets the density of my Hobart hood is located on the left upper part of the
helmet. The part that
was pointing up in my cramped area of work. It hit on something and was turned from 9 (my normal
setting for light duty MIG) to above 12.. Very dark for a weenie arc.
I retired
for the night at this point.
I was a little shaken by this episode and it was difficult to compose
myself for sleep.
I had
planned on putting the events of the next day plus some medical issues in this
report but it looks like they must wait till Test&Tune 179 is prepared.
More to
come.
Rick
Draganowski
(on fire in
Oregon)
Subject: Rustpuppy Test&Tune 179
Date: Saturday,
September 06, 2003 12:42 PM
Despite
the excitement of the previous night I awakened refreshed at about 5am. I had managed to finish my interrupted
sleep. I was anxious to get to work
but I knew I should take my time and I had all day to do the few things that
needed to be done to get Rustpuppy back on the road.
First I
crawled under to inspect and grind the work done last night. It looked a bit strange due to
the blind welding but there was plenty of good metal in the joint and I could
race the piss out of the Pup in this state. The proper finish welding could be done by
old Tim Harding at any time. See t&179-1.jpg and t&179-2.jpg
for the welds done before the excitement started last night.
At first
I was so anxious to get Rustpuppy back on the road I planned on just swapping
the street tire with the Drag Radial and getting her off the jacks. But that still small voice of sanity
insisted on freeing up and repairing the stuck brake drum on this side. So I spent considerable
time fixing this as reported about the other side.
Then the
old street Radial T/A went on and it was time to get Rustpuppy down from the
jackstands. The piddly
little two day job of tacking on the cutouts had taken old, slow Draganowski
about 3 months. But I
had some excellent excuses.
I took
my time on getting Rustpuppy down from the jackstands and she was finally back
on the ground in just before noon.
It was a welcome sight. See t&179-3.jpg.. I thought briefly of putting the Moons back now
that she was back on 14” wheels.
But I had gotten used to the “Road Warrior” look and will just clean up
and paint the great wheels that Rob Roberson donated to the Pup.
Then it
was time for a test drive.
The added volume of the closed cutouts added to the exhaust pipes have had an unexpected side effect. Rustpuppy’s exhaust note is
quieter and more mellow.
Really beautiful. I will
not open the cutouts until I can make a recording of it to share with the list.
I only
had a gallon or two of gas left so I knew I was limited to just a quick drive
on the old road. I
took it easy to get Goody warm and happy. After a bit of sane driving I did the Alan thing and
punched the throttle.
Since the Q-Jet mod that allows the secondaries to open immediately is
still in place the hard hit put Rustpuppy sideways in a cloud of smoke. It smelled and felt great.
At this
point hitting the throttle hard just blows the street tires away on any of the
surfaces I tested. It
is great fun. I had to
share. I knew that my new
neighbor was a bit of a hot-rodder from the conversation we had when I went up
the hill to pray this morning and met him walking his Dalmatian. So while I still had
a bit of gas left I headed up to his house on the hill above me. I just sat in his drive with the
Pup idling as his dog was going nuts
I did a
couple roll on launches with about 20 feet of wheelspin at launch and another
20 or so at the second gear shift and Russ was having as much fun as me. Then I did a couple full
throttle Alan style sideways launches and he was laughing out loud. I knew that the Pup
was out of gas so I got Russ back home.
I could coast home from there in a pinch.
He
wanted to talk about his cars and rodding and the Pup and everything in the
world so we yakked away for a couple hours.. He has a 55 Chevy with a 454 in it. (back in Arizona, his winter home) And he is a nut about chrome
plating and restoration so it must be a work of art.
It was a
great time..
Now for
something a little less fun.
I have been debating myself as to whether I should share another health
related issue with the list and it looks like I will inflict it on you all. (whining and
complaining is my specialty)
As you know I have arthritis. One of the results is that my feet are twisted
and crippled and despite special orthotic shoes I get pressure sores on my feet
and toes.. (I have other
problems from the arthritis in my back, right hip, hands and wrists, right
shoulder, neck but the hip and the feet are the worse.) The pressure sores are a chronic
problem for me. I must stay
active but there is a price to pay.
A couple
weeks ago one of the sores got infected with one of the nasty 21st
century bugs. It was scary
how fast the infection worsened.
I was lucky to have some great high tech antibiotics on hand (samples
from Dr. Williams) or I would have to go to the emergency room. And they would probably
have flown me to the trauma center in Rogue Valley Medical Center to avoid
legal issues. By the
time I got there I probably would have been in danger of losing my foot..
Damn..
But the
high tech antibiotics worked and I got a prescription for plenty more. I have been taking care of the lesion,
draining and bandaging as well as close monitoring.
Dr.
Williams advised me to stay off my feet till the lesion was healed but I
thought I could get away with some Rustpuppy work as described in this and the
two previous reports.
It was stupid and stubborn. I am sure that it interfered with proper
healing.
The
infection did a lot of damage and the arthritis deformed knuckle bones of my
toe are exposed and it is best to leave them uncovered as scar tissue
forms. So I have been stuck in bed
the last few days and cannot safely walk anywhere. I am angry with myself again so please don’t lecture me
about my stupidity. I
will try to do better in the future.
More to
come.
Rick
Draganowski
(fun mixed
with misery..)
Date: Tuesday,
September 09, 2003 5:40 PM
Still
stuck in bed. And the
rains have started. Couple
inches since
I did
some research on healing my foot lesion and decided to change my treatment
I have
been staying in bed as much as possible but had to get to town yesterday to see
Doctor Williams. He was impressed
by the great healing response I got from the new protocol and told me to keep
using it.
I picked
up 5 gallons of 92 octane and a bunch of groceries after the doctor visit. Put the gas in Rustpuppy today
and checked the tire pressures and fluids.. I was itching to drive the Pup again. But it had rained this morning
and the roads are still soaked..
But you know me.
I had
left the window open so when I sat down in Rustpuppy it was cold and
Sideways
at 40 on a crappy old farm road always increases your pucker factor. I haven’t disabled the instant response
mod of the secondaries so the Pup is a bit too sudden for safe driving in the
wet.
When I
got home despite my promise to not open the cutouts until I could share
Then I
jumped back into Rustpuppy and sat in the water again. I revved Goody up to about
4500-5000 and was amazed to find that she is not uncomfortably loud. Since the pipes open straight out the
sides most of the sweet noise goes out away from Rustpuppy. I am really looking forward to
some open exhaust testing on Rustpuppy Run..
I have a
problem with the microphone input on my new HP laptop and it seems like
Does
anyone have any suggestions on getting it working??
It will
be drying out starting tomorrow (the rains are not the miserable
Rick
Draganowski
(sideways in
Oregon)
p.s. I wonder of it would be correct to call
Rustpuppy a “Twenty-first Century Rat Rod”??
Subject: Rustpuppy Test&Tune 181
Date: Saturday,
September 13, 2003 4:24 PM
I am supposed to be in bed.. Still have a ways to go on healing the foot but
I had to get out and about to fetch water and do dishes and other chores so I
started thinking. It was hot this
afternoon (only about 80 but the roads are hotter than the hubs of hell from
the northern summer sun.
The wind was moderate with gusts to about 20mph .. Mostly from the north so it
wouldn’t interfere with a run..
I quickly fetched a piece of masking tape and got the secondary
delay vacuum pot working again. At the top of the hill I tried a few launches
with Rustpuppy to see what would happen with the sorry old BFG street
tires. As I suspected
there was a 0.3 second delay for the secondaries of the Q-Jet to open and then
the tires blew away.. Damn,
not the best response for racing..
Pressing on regardless I motored down to the end of the old road
for a zero to sixty run.. Tires
kept blowing away in first and second and I had to work the throttle to stay on
the road.. Miserable time of
6.24 seconds.. And lotsa
smoke..
At this point I should have just gone home. Yeah, right..
Waiting at the entrance of Rustpuppy Run it seemed like everyone
in the USA was using highway 101 today.. Giving up in disgust I motored down to the
south launch area.. I
stepped on the gas a little just to warm Goody up and the Pup was going about
100 in no time.. Then it was time
to lurk at the south entrance waiting for a break in traffic.. Finally one came. But rounding the corner at the
beginning of the Run I could see three damn motor homes lined up coming my
way. I just stopped in
the damn road at the launch area and waited for those 40mph turtles to pass. Then it was time for a run.
My nerves were good but I didn’t expect much.. After the 0.3 second
delay the tires took off smoking and I was pedaling the throttle trying to get
traction back. Got it and
then when I got back on it they blew away a second time.. This is not going to be a
good time with me stopping twice after the launch..
Finally Rustpuppy got enough traction to get going. It felt great to be back on
Rustpuppy Run doing what I do.. The time was terrible as I expected. 13.92@103.8
on the G-Tech..
But I was amazed that Rustpuppy could stay in the 13’s after stopping
twice during launch..
On the way home I did some g-force readings. Best I could get with throttle
modulation was 0.71 G but normally the tires blew away at about 0.6 G. The traction issues with the street
tires is aggravated by having 30psi in them instead of the proper 22psi race
setting. And about 150 lbs
of stuff in the trunk and gas tank is needed to hold them tires down.. Rustpuppy is running light
for the Drag Radials and I haven’t loaded her back up.
Normally the Radial T/A’s
need half a tank (about 60 lbs) or more of gas plus the 85 lbs of trunk
junk and the tires at 22psi to stick to the road at all.
Goody is running better than ever, the gas is good, tuning seems
perfect and the cold air system is working great.
I ordered the Firestone Indy 500 235/60-14’s a couple weeks ago
and expect them any day.
Hoping for good things from them after breaking them in.
.
Back in bed now and working on Rustpuppy Test&Tune Chapter
10 and this report.
More to come.
Rick Draganowski
Subject: Rustpuppy Test&Tune 182
Date: Monday,
September 15, 2003 7:06 AM
Yesterday (Sunday) when I went out for chores (Doc Williams said
it is ok to be up and about for a couple hours each day) I carefully checked
the weather.. It was about 11am
and the humidity was low with a temperature of 70 degrees. Wind from North about 15-20 mph. Good weather for a run.
I slowly loaded the 85 lbs of trunk junk back into
Rustpuppy. Then adjusted the
rear tire air pressure down to 22psi. Wish I had another 10 gallons of gas. (60 lbs) The Pup only has about 5 gallons in the tank now.
Then it was time to hit the road. At the top of the hill I did a practice
launch. Considerable cold bog and
0.71G of acceleration. Then I did
a 0-60 practice run at the bottom of the hill. It was much better at 4.8 seconds. There was just a slight bog and a
little wheelspin.
I lurked at the North entrance for quite a while but the traffic
was miserable for a Sunday morning. I really wanted to do a Southbound run (no
salt rime on the road and favorable wind) but finally gave up. Damn. Motored to the lurking area on the South end. It seemed like a big enough break in
traffic for a run. But a car
appeared about 200 yards behind after I got onto the Run. Went ahead and staged
anyway, since I figured the Pup would be able to stay well ahead of it.
My nerves were steady despite the distraction (they have been
better lately, wonder why?) and the launch proceeded normally.
But.
The salt rime on the South end from the surf driven by the fall
winds was too much. Damn
street tires blew away with amazing ease and I had to throttle way back to get
them to grab again. Seems
like I was just sitting there for a long time (just a fraction of a second, but
my time sense speeds up when I go racing) just fooling with the launch. The
BFG’s finally settled down at partial throttle and the run went on. I have picked up the bad
habit of lifting prematurely but I stayed on it this time. The Pup was probably pulling
about a 125mph air speed against the wind before I lifted.
The time reflected both the bad launch and the wind with a
reading on the G-Tech of 13.81@106.6. It probably would have been about a 13.5@108 with better traction and no wind. (like a
Southbound run) But it was still
great fun.
On the way home I did several more g-force readings at the top
of the hill. Since Goody was warm
and happy they were poor at 0.59G, 0.64G, and one at 0.68G. I was just rolling on the throttle for
these and the last one was taken during some wheelspin.
Now for something completely different.
Craig Hauber is sending me a device to allow higher quality
recordings of Goody music.
But due to my stubborn/stupid nature I decided to open the pipes and use
my kludgy audio pre-amp gizmo.
It does not have a fraction of the dynamic range needed to properly
record open cutouts but I will fool with it anyway. Since I opened the pipes (couldn’t hold myself back any
more) and I promised to share it became necessary.
Attached to this letter is open1e.mp3. This recording was made from about 12 feet
behind Rustpuppy and centered.
The audio level is enough to give some indication of the idle
sound. (but it is way louder)
Then in addendum 1 we have open2e.mp3. This one was made about 10 feet out from the passengers side
pipe outlet.
Audio turned down to just a tiny percentage of reality to accommodate
revving Goody to 6200 rpm. It overloaded
and distorted anyway.
Smooth huh?
Turned down the audio pre-amp even more for the next recording.
(in addendum 2) Open3e.jpg is back
centered about 12 feet behind Rustpuppy. Goody revved to 6200 again.. I love the sweet sound but
it almost hurts it is so loud.
Thinking about going racing with the cutouts open but don’t know
if I got the nerve. I
must go to town this morning so I will put a couple gas cans in the Suburban
for Rustpuppy. Racing seems
to use it up fast.
More to come.
Rick Draganowski