Subject: Return of Rustpuppy report 59
Date: Friday,
September 08, 2000 8:52 PM
Important
trip to town today so I fetched two 5 gallon gas cans (why do we call them
cans? they are made from plastic..
hmmm..) of 92 octane gas for ol’ Rustpuppy. You remember the last time she ran (just across the yard)
she ran out of gas and I used the mower gas (80 octane or so) to get her to the
motor transplant area..
Goody would spit up on the cheap stuff..
And I
got a chance to go to NAPA and bitch about the boot toasting on ol’ number
6.. Peg took pity on me and
gave me 4 standard boots off some salvaged wires.. Cool..
Later a bit of WD40 to loosen them up and the skinny guy was on ol’
number six.. (with 3 replacements
if any more toast) (See ror59-2.jpg)
I
devoted some time to getting the Q-Jet into place on Goody and taking care of
some details.. (ror59-1.jpg and
ror59-3.jpg)
It looks
like this weekend Rustpuppy will be running..
I have
been going back and forth on ordering the front tire replacements for
Rustpuppy.. First I want the
Big-N-Little look with 215/70-14’s on the front and the 245/60-14’s on the
back.. Then I want the big meats
all around, then I want the Big-N-Little... Yesterday I got so silly about this that I almost
ordered two of each so I could swap back an forth.. (I cannot really afford to
do that, old idiot..) Today cool heads and careful plannning took over for the
emotional see-saw.. If I
save up a little I can put a pair of BFG Drag Radials on them extra two 7”
Rallyes to improve the traction problems I see coming.. So I finally made up my mind and
will have the skinny meats for the 6” rims on the way next week..
Hmm... Do the Drag Radials come in 245/60-14???
More to
come.. For sure..
Rick
Draganowski
(getting to
the fun part..)
Subject: Return of Rustpuppy report 60
Date: Saturday,
September 09, 2000 8:36 PM
Some
details on Goody first. The fuel
line to the Q-Jet went on, a nice rubber one covered with aluminum foil
tape. Hooked up the vacuum
advance, and plugged the vacuum ports left over. Then I salvaged the grommet out of Knocker to hook the
breather tube to the air cleaner up..
I spent
time this morning making a checklist so there will be no screwups. (I hope)
The
column shift mechanism seems to latch into park so I just disconnected the shift
rod so it would not dangle.. Then
the shift lever came out like a bad tooth.. Moved the tachometer (old original Sun Super Tach II) so it
would be in the right place in park..
Then
moving on to the instruments.. I
disconnected and removed the old JCWhitney triple electric gauge. (with a bad
temp sensor and oil press sensor.. bah..
6 years and it is trashed)
Then
sitting there in the drivers seat and trying different locations for the big
mechanical AutoMeter gauge set I came to the conclusion that the dash pad had
to go.. Aided by Dave M.’s disco
dash removal I proceeded in my own style.. See ror60-1,jpg for the initial gnarf and the tools used for
the removal..
Ror60-2.jpg shows the result..
I also removed the air conditioner ducts and the heater/AC controls
using similar techniques to cleaning a very big fish..
Then I
flanged up a nice mounting bracket for the AutoMeter gauges and got it
attached.. (being very careful not
to bust the windshield during the hammering part.. Too dark for pictures, so see tomorrows report..
I
determined that the temp bulb and fittings were identical to the smaller gauge
used on the Goody test stand. (was
hoping that was the case as the adaptor is still in the head and the header has
to come off to change it..)
Then I
found out that the nice ¾” hole I made in the firewall back in ‘94 was too damn
small to get the water temp bulb fitting through.. Autometer sez use a 7/8” drill.. So that is where she sits till
tomorrow..
In spite
of my resolve to be calm and
methodical this weekend the tension and excitement is building up and making it
difficult to work in a relaxed and measured way..
I tore at
that dashpad like an animal..
Grrr..
Rick
Draganowski
(nervous and
excited..)
Subject: Return of Rustpuppy report 61
Date: Monday,
September 11, 2000 9:19 PM
Squeezed
out just a couple hours yesterday and two more today. The instruments (neato AutoMeter 2 5/8” mechanical set for
70 bucks) were mounted and hooked up properly.. (ror61-3.jpg)
They warn you that if you hook up the voltmeter backwards
it will damage it.. Strange. I have never seen a voltmeter damage
itself from incorrect polarity..
The radiator went in and all the hoses hooked up. It is not a bleach
bottle but a non-toxic soap bottle from Canada.. (ror61-2.jpg and ror61-5.jpg)
I noticed
that a love tap Rustpuppy did on one of my trees back in ‘94 pushed the right
shock absorber thingie in about ½”..
(was reading and slowly rolling till the tree jumped in front..) So I salvaged a virgin relatively
rust free one from Yakima Sue..
(ror61-1.jpg)
Come to find out that the 3rd bolt (capscrew
down through the frame to secure the rear of the shock) was rusted in solid and
that the inner fender panel has to come out to provide access with the air
wrench or breaker bar. I
want to put the bumper and grille back on before I start running around in
Rustpuppy as she looks too much like a car which deserves a ticket with the
naked front end. (ror61-4.jpg)
Did some
cleaning up and painting in the trunk getting ready for the battery
installation. There was a lot of
other cleaning and painting as well..
Just don’t remember the details..
I was
all worked up and nervous because I fully expected to get Rustpuppy on the road
last weekend. But the Nova work
time just was not available. I
have backed away from making any promises to myself or the list about just when
it happens.. I will be taking my time
and steering clear of the tensions associated with scheduling.. There are already too many
deadlines in my life..
So, it will be “real soon now”. and not sooner..
More to
come...
Rick
Draganowski
(laid back
and mellow..)
Subject: Return of Rustpuppy report 62
Date: Tuesday,
September 12, 2000 9:48 PM
Since I
have come to my senses about being in a hurry to get Rustpuppy back on the road
I have been making slow but steady progress without the stress.. I have resolved to clear away most all
of the details which would probably be neglected the minute ol’ Rustpuppy is
back on the road..
The
replacement front bumper shock was the first issue.. (note length difference ror62-1.jpg)
I made a tiny mod in the inner fender panel to provide
acess.. (ror62-2.jpg, GM shoulda
done it..) When the bumper
is off is the best time to replace these..
You can
see the heavy Disco bumper about to be rassled into place without busting off
the plastic facia wingie thingies.
Seems like more than 70lbs..(ror62-3.jpg)
And then magically (after getting twisted into a pretzel getting the nuts on) right where it belongs.. (ror62-4.jpg)
The grille
went on in a trice and that was the last of the front end stuff..
Purdy.. (ror62-5.jpg)
I
cleaned and painted the battery area in the trunk and got the battery back
home.. You will like the terminal
bolts I am using..
Then I
decided that something MUST be done about the great big hole in the
transmission tunnel.. So I
sat in Rustpuppy sidesaddle, idly scraping up mastic gum with a putty knife,
and thinking of a neat way of dealing with “The Hole”..
I have a
nice piece of 7075 alloy aircraft aluminum sheet.. Hmmm.. So I
planned on cutting out a nice rectangular piece and then putting it in place
with a bunch of sheet metal screws..
I ground away on that issue till darkness caught me 2 screws short of
being done.. (20 all together)
Pictures tomorrow..
More to
come...
Rick
Draganowski
(calm
and quiet.. only one little
fit of “urgent” workin today but got it under control..)
Subject: Return of Rustpuppy report 63
Date: Wednesday,
September 13, 2000 8:43 PM
A
pleasant surprise was waiting at the front door of my shop when I was getting
ready to go to town today. The two
BFGoodrich Radial T/A’s for Rustpuppy’s front wheels were here already..
(ordered them Monday) With second day FedEx shipping from Nevada the total bill
was $121.13..
So I
rummaged the old wheels and tires out of the Dawg and threw them and the new
tires into the back of Patches..
I figured on dropping them off at my favorite 76 Station and having them
mounted and balanced while I took care of business.. That worked out perfectly (cost 20 bucks)
and I came home with them ready to put onto Rustpuppy to replace the cornered
off sorry tires on the front..
These are 215/70-14’s for the Big-N-Little look with the 245/60-14’s on
the back.. They have the exact
same diameter though.. Nice..
See
ror63-1.jpg and ror63-2.jpg.. The
ends of little steel wires are just starting to stick out on the old
tire.. Not good..
Ror
63-3.jpg and ror63-4,jpg show both sides of ol’ Rustpuppy proudly wearing her
new front boots..
By the
time I got the wheels changed the light was gone and Nova work for today over..
Tomorrow
looks to be another day when real work will probably wipe out any Nova
work.. Sigh..
Anyway, some
progress was made..
More to
come..
Rick
Draganowski
Subject: Return of Rustpuppy report 64
Date: Thursday,
September 14, 2000 8:21 PM
As I
predicted yesterday the time for Nova work was at a minumum but I did manage to
get the last 4 sheet metal screws into the cover for “The Hole”..
Looks
pretty good and it is removable..
In case I want to mess about with the governor..
Also I
managed to get water into the radiator..
Just plain water till I am 100% sure that there is no way for coolant to
get into the oil pan.. Antifreeze
is really bad for bearings.. (read
that in Chevy High Performance
tech tips or mebbe somewhere else..)
More to
come..
Rick
Draganowski
(slow
and steady.. and a little
impatient from time to time..)
Subject: Return of Rustpuppy report 65
- Rustpuppy Returns!
Date: Friday,
September 15, 2000 8:59 PM
A
grueling day on the project (not Rustpuppy, real work) but it finally ended and
much was done. My associate Dave
Sorensen stayed an extra half hour to help me get the hood back on ol’
Rustpuppy.. Believe me, it is a
lot easier with two than by yourself..
So after
that (about 6:30 or so and it starts gettin dark at 7:45) I had a teeny window for some more Nova
work.. First things first, I
got 5 gallons of the 92 octane into the tank. Then I attached the battery and the moment to have Goody
come to life in Rustpuppy came..
I did
not really adjust the static timing since I expected to have the hood off for
that so I figured I could wing it..
I had a good mental image of where the distributor would be for about 8
degrees initial and set it there.
(leaving the hold down bolt just loose enough for tweaking while
watching with the timing light later..)
Clearing
away some tools to make room, I sat behind the wheel and cranked her
over.. It didn’t take long
as there was already some gas in the float bowl from running on the test
stand. Goody sprang eagerly
into life. The oil pressure came
up to 55lbs and everything sounded good..
Real good.
I sprang
out quickly leaving Goody on high idle (about 1200rpm) to check for gasoline or
water leaks and everything looked perfect..
I had
already put 4 quarts of the Ford fluid into the tranny (as B&M recommended
for startup) so I got busy and put 3 more in before it showed on the
dipstick.. Then two more and I got
back into Rustpuppy and shifted the transmission through all the gears to purge
the air internally.. It took one
more to bring it up to the full mark..
When I was fooling with the tranny fluid I was starting and stopping
Goody by just reaching in through the window.. Flawless starting..
Just a tiny fraction of a rotation and she would spring into life and
idle happy at about 900rpm with a lovely lope..
At that
point I thought Rustpuppy was ready to roll... I got back in..
Fumbling with the unfamiliar (yet) Pro-matic shifter I got her into
reverse and started backing across the lawn.. Then when I first began to turn I could tell that I did not
have the power steering working..
It seems ol’ idjit Draganowski spilled out most of the fluid from the PS
pump reservoir when he was fumbling with the fittings to put the hoses back on
the PS unit.. It took about
¾ quart to bring it up to just a little too much.. Then starting up and running the wheel lock to lock a couple
times and everything seemed to be working..
So It
was back out across the lawn and gingerly turn out into the old road.. (lots of places to hang up the new
Dynomax headers.. remember the
dents in the old FlowTechs..)
Then it
was Seat Time!
Cruising
down the twisty old road (which ate the old tires) and varying the throttle and
listening to the music of the pipes.. It has been a long time since the 19th of
December 1999 when Rustpuppy took her last ride and the knock started..
Everything
sounded and looked fine (45lbs oil, 170degrees water, 14volts) and there was
just a little smell from hot pipes burning out the creatures which had moved in
over the last 9 months..
Curious... 9 months almost to the day.. Same as a baby..
I will
be getting the timing set and then after another 4 mile run changing the oil
and filter.. Then retorque the
carb bolts and try to get the interior finished and probably a dozen more
thingies which need doing..
More to
come, with pictures, tomorrow..
Rick
Draganowski
(getting
to the fun part, the really fun
part..)
Subject: Return of Rustpuppy report 66
Date: Saturday,
September 16, 2000 8:58 PM
Last
night after dark I could not help myself and snuck out for another little run
with Rustpuppy. With the lights on
I noticed right away that the AutoMeter gauges were TOO BRIGHT. The rheostat in Rustpuppy’s dash
had gone to its reward about 3 years ago so the instrument lighting was in a
binary mode.. Either off or on..
I
fumbled out the silicone rubber lamp covers provided and first tried the red
one.. Still too bright and
looking like something you would see in the window of a cathouse.. Then the green.. Still too damn bright.. Hmmm.. Then I put the red over the green and tried that.. Not bad.. Not greenish red but sort of rust colored (how apt..) but
about the correct intensity..
So rust
colored instrument lighting it is..
After
going on the short run (4 miles) I came to the conclusion that the Pro-matic
shifter was not working right..
Going up from park (PRND21) everything seemed to work.. But going the other way from first gear
position (which is pushing the cable instead of pulling) neutral was still
drive, reverse was neutral and reverse happened half way down the park
detent.. Hmmm...
It looks
like the slop (mechanical latency) in the system was excessive..
Went to
bed thinking about this stuff last night..
This
morning when I could finally drag
my creaking old bod out to see about Rustpuppy I attacked the shift slop
problem first..
Jacking
up Rustpuppy and sticking a jackstand under gave me room to reach up there and
find the lever and cable stuff on the tranny.. Since the headers and pipes are on there is no direct view
so it is a paw around kind of job..
I had the shifter in the neutral detent and I knew the tranny was in
neutral (tested it before blocking and jacking. So it was just a few seconds work to get the nut off,
insert the two washer slop fix I came up with a couple weeks ago and button
everything back up..
Testing
after proved the principle and the shifter can downshift and upshift manually
just fine in all gears now..
Itching
for more seat time I went on a short run to check everything out and it was
cool..
Later
today I got the urge for going on a “long run”, (about 10 miles total and
including Rustpuppy Run..)
On the
way back across Rustpuppy Run I kinda stepped on the gas a little more than
moderately and went from a sedate 55mph to a wee bit over 4000rpm.. (about 96mph) It happened a lot faster than I was used to.. Whoo Haa! Nice passing gear..
When I
backed off after the full throttle mini-run and generated lotsa vacuum I saw a
considerable cloud of smoke emanating from the right pipe.. I wonder why and why just the right
pipe..
There
are lots of little strangenesses to get used to or to worry about.. For instance, with the new g-forces
when the gas tank is low the pickup is getting exposed sucking air and causing
a lean out miss.. I put the other
5 gallons in today because of just that concern.. But I am not too worried and will just have fun till Goody
is broke in nice..
The
biggie which I will be thinking about tonight is the poached egg feeling I got
after the long run.. The headers
get the floor almost hot enough to fry an egg on.. I had been planning on just a plain painted metal
floor for Rustpuppy but that idea may have to be discarded.
I will
not have a carpet in Rustpuppy but I really need some quality insulation.. Hmmm.. Mebbe something on the bottom of the floor thermally
isolating the headers and
pipes. It gets really hot under
there..
What
would be good for that??
I still
haven’t adjusted the timing properly and promise to do that tomorrow for sure..
The oil
change will have to wait as Goody is wearing the last oil filter from the last
case I bought and I was too stupid to buy another case of them last week.. Duhh.. Monday for sure.. Plenty of oil but no filters in stock..
More to
come..
Rick
Draganowski
(Rustpuppy
goes fast and sounds really good..)
Subject: Return of Rustpuppy report 67
Date: Sunday,
September 17, 2000 9:29 PM
As
promised yesterday the first order of business was getting the timing set
properly.. After much farting
around and getting Goody to run “Like Ass” I came to the conclusion that the
distributor centrifugal advance springs were too soft.. The weights in the ProForm distributor
must be heavier than I am used to..
What was
happening was mostly related to idle ability.. The advance progression would speed up the idle enough
to cause more advance.. It was an
unstable positive feedback situation with poor Goody either dying when put into
gear or spinning the tires..
I came up with a reasonable combination of idle throttle setscrew versus
initial advance to allow driving but it is an uneasy compromise.. Tomorrow the other heavy spring goes
back into the distributor and the whole process repeated..
Other
challenges presented themselves..
Checking the number six spark plug boot finds the new skinny one toasted
too.. Bummer.. Will measure the actual distance
between the end of the plug and the damn pipe.. (which I suspect was welded in wrong.. Cheap help..)
And the
right pipe is blowin blue smoke in a random kind of way.. Mostly under load but not always.. Weird.. Just ring seating I hope..
And last
but not least I am running out of gas again.. It seems like the motor will pull like crazy till it uses up
the gasoline in the float bowl (which ain’t much in a Q-Jet) and then poop out..
Will
change the filter in the Q-Jet but I suspect the pickup sucking air due to having
used up about half of the 10 gallons I put in.. In just 40 miles of spirited driving.. Hmmm... Really need to go to town for a fillup.. It was a fun 40 miles though..
We had
the hottest day of 2000 today so the “Poached Feet” syndrome was a serious
factor.. I did some
crude testing and determined that the whole floor is getting hot with serious
hot spots above the headers and pipes..
I had idly thought of just insulating the tops of the header collectors
and exhaust pipes but it looks like Rustpuppy really needs total floor
insulation and, I dread to say, a carpet..
I know
nothing of such things and really need help on just exactly would do the job at
minumum cost..
How much
does stuff like that cost? You
know, I have never looked..
More to come..
Rick
Draganowski
(Seat time
is good, even with poached feet..)
Subject: Return of Rustpuppy report 68
Date: Monday,
September 18, 2000 9:43 PM
Since
the timing advance problem has Goody running “Like Ass” and complicated the tuning
beyond my ability to resolve I decided to get the spring change in the ProForm
distributor ASAP today.
Ror68-1.jpg
shows the distributor field stripped and ready for surgery.
You can see the weak sister spring on the right which has caused me so much trouble.. And look at the fat weights.. (ror68-2.jpg)
The best tool to use on springs is a genuine TeleType
corp. spring hook..
(ror68-3.jpg) I been
carrying this one around since 1969...
Ror68-4.jpg
shows the proper spring back in place..
Quick and easy if you got long arms..
The
temporary and expedient fix I put on the cut out radiator support frame (read
halfassed) turned out to be less than totally successful.. (read total failure, I am lucky the
radiator didn’t go into the fan)
The proper and secure fix went in next.. (see ror68-5.jpg and ror68-6.jpg)
Then it
was time to fix the toasted boot problem.. (ror68-7.jpg)
The actual distance from the end of the sparkplug allows a
25/64th drill bit but stops a 13/32nd job. (less than 0.406 but more than
0.391) Not much but more than I
thought but since the pipe is offset in the direction I want the wire to go it
toasts the boot. Putting a Tyrap on the plug to hold the boot at a sharper
angle looks like a workable solution..
(ror68-8.jpg)
Note the
black RTV trim cement holding the red nozzle thingie on my WD40..
I always
used to lose those..
With all
the ducks in a row it was time to get to the timing and idle adjustments.. Everything worked like I was used to
and it was a pleasure compared to the nightmare I had been having with the
out-of-control centrifugal advance.. I have Goody set for 12 degrees initial advance with
32 total centrifugal. The vacuum
can is set for only 10 degrees.
I went
out for a test drive but it had too be a short one as I am running out of
gas.. I stole a gallon for the
mower out of the 10 gallons of gas for Rustpuppy so the 9 I started this
adventure with is fading fast..
Probably don’t have enough to get to town for a fillup.. What an ol’ idiot I am sometimes.. Just couldn’t keep my big size 14’s out
of the throttle..
The 1
mile test drive was fantastic! Not
“Running Like Ass” any more!
Happy
happy, joy joy!
I had
time just at dusk to flange together a neat solution to the poached feet
problem.. But that issue can wait
till tomorrow..
More to
come..
Rick
Draganowski
(having too
much fun to be possible..)
Subject: Return of Rustpuppy report 69
Date: Tuesday,
September 19, 2000 9:02 PM
I
threatened yesterday to reveal the solution to the toasted feet problem.
And that
is the business at hand today..
I
started with some special high quality double corrugated board salvaged from
the large boxes Stihl ships it’s bulk chainsaws in. (chainsaws is big business here in Gold Beach)
Cut it
out to fit the floor..
(ror69-1.jpg)
Then
using the neat double aluminized building paper the cardboard is covered on
both sides and taped with aluminum foil tape. (ror69-2.jpg and ror69-3.jpg)
Then I cut
a large piece of aluminum flashing material and taped it down with the aluminum
tape. (ror69-4.jpg) This is to protect the paper and
cardboard from my big size 14’s..
I
painted the rusty parts of the floor with gray primer.. That is all I am doing on the
passengers side. They will have to
live with toasted feet.. Then I
attached the electric defroster with double stick tape.. The stuff that is used for new car trim
installation..
The dash
was quick and easy.. Just a piece
of the aluminum building paper (about the thickness of the cardboard used in a
telephone book cover) cut to fit, painted flat black, and stuck down with
double stick trim tape..
Then I
sealed the extra big hole where the Pro-matic cable went through the floor with
a piece of aluminum flashing and some more of the aluminum tape..
Ror69-5.jpg
and ror69-6.jpg shows the finished (for now) interior.. Need them seat covers..
The
miniscule seat time today showed a disconcerting popping in the headers.. I suspect a fouled plug as a touch of
the gas cleared it up and Goody is pulling really good.. There is a possibility that there is an
ignition problem as I have heard negative stories about the ProForm HEI
ignition module.. I am
itching to get some more gasoline so I can put some serious miles on
Rustpuppy.. There is
only 44 miles on the odometer since she first moved on the 15th..
Will be
buying a spare NAPA ignition module and keep the tools necessary for a change
in Rustpuppy till I get to the bottom of the popping.. I am thinking of the cutting out at
speed (like someone turned off the ignition) problem as well..
More to
come..
Rick
Draganowski
(fun with
aluminum tape..)
Subject: Return of Rustpuppy report 70
Date: Wednesday,
September 20, 2000 9:15 PM
Lots of
little odd ends which I haven’t covered in the regular reports due to excess
excitement. As you remember I
Rustpuppy was suffering from an assortment of electrical gremlins which I
chased my tail on for many months..
And as you also know I had to reorganize the 10SI alternator salvaged
from the original six from Rustpuppy to install it on Goody..
Since
that moment all of the strange electrical problems went away.. I had been fighting a flakey
alternator and not connector problems.. It is nice to have bright lights and 14+ volts again..
The
Sheriff’s Association sticker on Rustpuppy expired last January and today I put
on the nice new 2000 job..
Believe what you will but Rustpuppy has been wearing one since 1993 and
it brings her luck..
Due to
my excessive throttle usage the 9 gallons Rustpuppy started this adventure with
has dwindled down to about 1 or 2..
Not enough to get to town for a fillup.. My associate Dave, who has been working with me,
volunteered to bring back 15 gallons of 92 octane tomorrow.. Hoo Haa! Looking forward to more seat time soon!
The
strange random popping in the exhaust and seeming ignition module problem is
still there but much less..
(I gave Dave a little ride today, having his 200lb bod in the passengers
seat helps traction..)
Because
of caution and bad reports about the ProForm modules (and a hint of paranoia(
today I put together an emergency module replacement kit with:
Distributor
wrench (you have to loosen the distributor to turn it to get the rear dist cap
latch open, damn!)
Timing
light (to reset timing you screwed
up getting the cap off)
screwdriver (to get the cap off, and the module
screws)
nutdriver
(for the high zoot brass contact rotor screws, not slotted, little hex head
mothers)
Echlin
(NAPA) known good module
The kit
resides on the passenger side floor..
Rustpuppy
has developed a serious banging in the rear due to the left side exhaust
loosening up and bouncing against the fender when the motor idles with the neat
lope.. Dave thought it was
funny it was so loud.. Gotta fix
that tomorrow..
Only 1 mile
of seat time today..
But...
More to
come..
Rick
Draganowski
(lotsa
little details..)
Subject: Return of Rustpuppy report 71
Date: Friday,
September 22, 2000 7:59 PM
Nothing
but “real work” till dark yesterday..
But today is back to Nova fun.
First I addressed the problem of the banging exhaust and found all the
nuts on the exhaust adaptor “flange up” loose allowing the weight of the
muffler to pull down and push the tailpipe against the fender.. What a noise it makes when it does that.
I
tightened them up but it is obvious that they need some kind of locking
mechanism.. Tomorrow I will get
proper working height on Rustpuppy and double nut with lockwasher inbetween
those nasty little boogers.. They
loosened right up after a few miles of seat time today..
Dave
brought the 15 gallons of 92 octane yesterday so after putting 10 in Rustpuppy
is flush with over half a tank of good gas..
Todays
initial run brought out the fact that Goody is troubled by three different problems.. Here they are..
1) the “running out of gas”
problem.. I am almost sure
it is the crummy little filter in the Q-Jet.. (it was)
2) the random missing and bangin in
the pipes.. Ignition for
sure and suspect the ProForm ignition module.
3) blowin blue smoke out the right
pipe.. Don’t know about this one
as it seems much to much for just rings not seating.. Am thinking that I have a leak in the intake manifold
sucking oil from the lifter gallery.. (or mebbe something more serious.. I hope not)
First I
addressed the “crummy little filter” suspect.. It was out in a jiffy.. It sure seems like a tiny little thing. I wonder what the Rochester engineers were thinking of..
I could tell that Goody was much happier with proper fuel
delivery in just the first few hundred feet.. When I got to the little run stretch on the old
highway I pushed her pretty hard in second gear looking for the “running out of
gas” syndrome.. I must have
gotten a little excited cause I made Goody pull at full throttle in second gear
right up to 6000rpm.. Hoo
Haa.. Not running out of gas
now! She was smooth as silk
at that rpm too.. It was pretty
exciting since that is about 91mph on the narrow little country road.. And it did not take long to get there..
You know
I was fighting that lousy little filter back last year when I was doing
Rustpuppy Log reports and was seeming to have a fuel delivery problem.. I did and was too stupid to think
of the obvious..
The
“random missing and banging in the pipes” is still present though.. Tomorrow I will swap out the whole
Proform distributor with the modified GM distributor which came out of
Knocker. If the missing and
popping goes away I will raise a little hell with the Proform folks.
I ran
Rustpuppy out on the highway (101) for the first time since Goody went
it.. I got her up to 4500 in third
(about 104mph) but just for a moment since it was too windy for safety at
anything over about 80 today..
The
smoke has me worried though..
For now I will stick with the assumption that it is just a stubborn set
of rings.. Besides Goody
only has about 55 miles on her..
It is too early to tell..
Got a
list of stuff to get at NAPA when I get to town.. First on the list is a proper in-line fuel filter..
More to
come..
Rick Draganowski
(still
going fast and sounding good, but
popping and smoking and banging too..)
Subject: Return of Rustpuppy report 72
Date: Saturday,
September 23, 2000 8:29 PM
Now that
the fuel delivery problem is worked out I addressed the random missing and
header popping problem which I suspect was the Proform 170 buck (high zoot for
me) polished distributor.
That
distributor has been a disappointment in many ways.. Like 60 thousanths end play and a really crappy 25
degree vacuum can.
I
started by bumping the starter to get the rotor pointing at ol’ number
one. Then the Proform was out in a
jiffy.. I tested acess to
the rear cap hold down latch but it is impossible without climbing on the cowl
area and that would be quite a sight if I tried it.. So loosening the hold down and turning it seems to be the
only choice I have..
It was
enought of a pain separating the high voltage harness assembly from the top of
the distributor cap.. I wanted to
make a clean sweep of the Proform and replace the coil as well..
Ror
72-1.jpg shows the two distributors passing in the night.. The knarly standard GM Delco Remy job
(original module from 1977 truck in it)
and the who-knows-where-it-came-from Proform.
Ror
72-2.jpg shows Goody sans-distributor waiting for the familar ol GM job.
And
finally ror72-3.jpg shows the job completed..
I set
the timing for 10 degrees initial with about 28 total for the testing.. I bet Goody will be happier with 16
inital and 34 total.. But first it
was time to find out about the popping and missing..
Hoopla! The test drive showed smooth as silk
running and none of the random missing!
That is
two correct troubleshooting guesses in a row! (that will never happen again.. sigh..)
But.. (why is there always
a but?)
The blue
smoke from the right pipe is still there to aggravate the hell out of me.. After the test run and with the
motor at operating temp I left Rustpuppy idling in park and crawled out to
watch closely..
Blue
smoke, (noticeable but not heavy) was coming out of the right pipe but none at
all from the left pipe..
And the exhaust beat seemed a little irregular on the right compared to
the left..
I wonder
if the assembly guys down in Mexico may have left a ring off or
something.. Nightmarish thoughts.. Damn.. I hope it is something simple like the
intake gasket..
There is
only about 80 miles on Goody now so my plan is to run her moderately for a
couple weeks and then go through the misery of trying to get a compression
check.. The right side headers
have to come off since the acess to the plug holes on that side is
blocked.. And that is the side I
got trouble with.. Bummer..
Oh
well, at least Goody is running
good and I will bump up the timing and do something about the exhaust loosening
up tomorrow..
Rick
Draganowski
(it is
always something.. worried about
the smoke..)
Subject: Return of Rustpuppy report 73
Date: Sunday,
September 24, 2000 8:33 PM
The
loose nuts on the exhaust flangeup were first on the agenda today.. I jacked Rustpuppy up one side at a
time (with jackstand under) and put a stack of lock washers and flat washers on
each stud.. That should allow a
bit of motion and yet keep constant spring tension against the nuts to keep
them from loosening up.. It
went flange, lock, flat, lock, flat, lock, nut. We will see if this does the trick. If not I will add another lock washer
on the other side of the nut and then another nut.. (see ror73-1.jpg (it is a poor pic since I was losing the
light when I got done grovelling around on the ground))
The
timing was next. I discovered that
the springs I put into the ol’ stocker distributor (Moroso middle tension) are
just a wee bit too weak for the happiest tuning.. It makes the idle adjustment too tender as the centrifugal
advance starts just a bit too early. (at about 1500rpm instead of 1800)
But it
settled down and seemed to be happiest with 34 degrees total advance.. I had to reduce the idle just a wee
more than would be good (it will die when cold and shifted into gear) so that
has to be sorted out tomorrow.. It
got dark and cold on me..
The seat
time was good today but the black cloud of concern over the blue smoke from the
right pipe seems to be taking a lot of the fun out.. Oh, well..
More to
come..
Rick
Draganowski
Subject: Return of Rustpuppy report 74
Date: Sunday,
October 01, 2000 6:39 PM
Strange
things started happening over the last week. I had about 90% convinced myself that the blue smoke
from the right pipe on Goody was caused by an intake manifold leak. So I had been getting stuff together
for the R&R job.
While
this was going on I was getting a little half-hearted seat time. (enough to burn about 10 gal of 92
octane) My concerns about the
serious looking smoke from Goody’s right pipe was draining most of the fun.
During
this time I was watching the coolant (plain spring water) levels as well as the
ATF and motor oil. Strange stuff was
happening. The oil in the tranny
was going down rapidly and the oil level in Goody was going up! At first I thought that perhaps
it was a combination of leaks.
Transmission pan gasket and water sneaking past the intake manifold
gasket. (which was under suspicion)
But a
couple days of monitoring the tranny showed no leakage at all. Not one drop. Yet it had lost about 3 quarts of fluid.. How? And when I changed the oil in Goody (140 miles on
first batch) there was nothing but clean nice oil there.. About 6 ½ quarts.. (supposed to be 5, I put 5 in..)
I had
bought a TH350 modulator last week to change just to be on the safe side. (and it was the last straw I was
grasping at to avoid the manifold job)
I had
never heard of oil in quantity being transferred like this but it had to be
so.. So when I pulled the steel
vacuum line off the manifold and pink Ford tranny juice ran out I was beside
myself with happiness.. I
was jumping around and yelling like a little kid.. (wonder what the neighbor thinks?)
So that
was it. The vacuum port which
services the transmission is located on the number 8 intake runner.. Poor number eight was eating a
lot of oil.. It was starting to
creep up the outside of the tailpipe in liquid form.. Wow..
The fact that it was winding up in the oil pan was amazing though.. Seems like no matter how many weird
things you see there is always another..
Yesterday
after work (serious construction
on my Deloris’ special new home) I swapped the modulator.. (see ror74-1,jpg for
the villain of the story) Too cool!
After running the piss out of Goody the smoke faded and
never came back!
I went
out after dark on Rustpuppy Run and let Rustpuppy stretch her legs a
little.. (about 4700rpm in 3rd,
108-110mph) At the end where I
turn around (a beachfront rest stop) there was a load of State Police
rollers.. Oh, oh.. When one of them came out right
behind me and hit the lights I figured my goose was cooked.. The old adrenalin started
flowing big time..
But it
was not. Seems that it was a
call about shots fired on the beach..
Poachers are running amuck around here and the State Police are the game
enforcement guys.. The
earnest young officer just wanted to ask me if I had seen any suspicious
activity in the local neighborhood..
I told him that there had been a lot of late night shooting and where I
been hearing it..
Whew! Not a traffic stop at all.. And the damned left taillight was out
After my
nerves settled down I drove back home like a little old lady..
Well
most of the way like that anyway..
Today I
checked everything again. The
tranny was stable and Goody was still about ¾ quart high.. (I better drain the extra oil..) The radiator was full to the brim
with spring water. Goody ran like
a clock during today’s seat time pulling hard and not missing a beat..
I opened
the petcock on the radiator and drained out enough water to make room for one
gallon of premium coolant (with aluminum corrosion protection for my
Edelbrock)..
I
figured the number 8 sparkplug must be fouled from eating so much tranny
fluid.. When I pulled it out to
replace it (one of the easy to get to ones) it looked peachy keen! The serious running had cleared
it right up.. (see ror74-2,jpg)
It is
all coming together.. The
idle is cool, the tranny shifts like a dream. Stays in first till you tell it to shift with the
Pro-matic.. Goes like a bat out of
hell.. Fun again..
Now I have
to do something about covering them rust holes before the rains start..
More to
come..
Rick
Draganowski
(the G-Tech
comes out of the Suburban glovebox soon, mebbe next week)
Subject: Return of Rustpuppy report 75
Date: Tuesday,
October 10, 2000 9:14 PM
Plenty
of quality seat time in the last week.
All the work and worry is paying off. Goody is running like a clock and when the time comes to
take the G-Tech out of the bag (I took the G-Tech out of the Suburban glovebox
and put it in Rustpuppy) I expect quite a pleasant surprise.. (G-Tech stays in the bag till 500 miles
is reached)
Rustpuppy
got to town for a fillup and I did the dumbshit driver routine with the turn
signals.. Motoring down the road
with my left signals on.. Duhhh.. I had installed the Extra Loud flasher
from JCWhitney through the dash so it was sticking through the old radio tuning
hole.. But I still didn’t hear it
and the gauges block the dash lights..
Damn!
In
desperation I cobbled up a little aluminum megaphone for the noisy flasher.. (picture
to come later) It seems much louder..
Time will tell.. It is a
combination of my failing hearing (damaged during my Air Force days) and
Rustpuppy’s loud pipes plus the absence of a rear seat or any carpeting..
Today
during seat time I fooled around with powerbraking to figure the stall speed of
the TCI Break-A-Way converter.
I could not hold the right rear from spinning using all my strength on
the brakes. It would bust loose at
about 2750rpm when the secondaries on the Q-Jet started opening.. It was a weird but happy
experience..
Also on
the southbound Rustpuppy Run section of the drive I was being cool at 60mph
with the windows all closed. I
decided to get on the throttle a wee bit.. The closed tin can nature of the interior combined with
the plain steel floor and loud pipes set up a resonance at about 4100rpm which
was actually loud enough to cause my left ear to hurt.. Very impressive.. Will do the fast stuff with that window
down in the future..
On the
northbound Rustpuppy Run I let Rustpuppy stretch her legs just a little.. Up to
4700 in 3rd... (about
108mph) It sure didn’t take
long to get there.. (window was
down)
A very happy
drive..
More to
come..
Rick
Draganowski
(the winter
rains are starting, bummer..)
END OF
CHAPTER 8