Subject: Return of Rustpuppy report 76
Date: Monday,
October 16, 2000 8:04 PM
Plenty
of small thingies since the last report.
I was concerned about the taillight sockets being too corroded for
service so I replaced them both. The
best I could get at NAPA were pretty cheap and nothing like the OEM jobs.. Everything is getting cheaper but
not less expensive..
While I
was checking out the work I discovered that the brakelights were not
working.. Driving that
way is just asking for it so I dug into the problem right away. Fuse was good. Voltage at switch. Nothing getting through switch.. Damn.. Not easy to change for an ol’ fat cripple guy..
I wanted
to get Rustpuppy on the road for more seat time. Thought about salvaging the switch out of the old white
truck.. Then it hit me. I have Yakima Sue (for parts) and the
Junkyard Dawg just sitting around.
So I sat
on the ground and reached in and slowly unscrewed the bad switch from
Rustpuppy. Then repeated the job
on Yakima Sue.. It was after dark
by the time I got the replacement in and adjusted but it is worth it to keep
Rustpuppy on the road..
I spent
a few minutes replacing the 25 buck clear Mr. Gasket distributor cap on the
Proform distributor. It seems that
the plastic used on the clear cap absorbs water and is useless for this
location. Tracy at NAPA tipped me
off on this. He had tried one on
his drag pickup and it gave him nothing but trouble.
Then I
installed the replacement NAPA module.
Just as I tightened the last screw I heard an ominous “snap” sound. Then I looked at the directions
on the little piece of paper in the box.
It said “Do Not Overtighten”..
Damn.. I think that I broke
the thermoplastic body of the critter..
Poop!
Thirty-some
bucks down the drain if it is fouled up..
I had
put the megaphone on the “Extra Loud Flasher” in Rustpuppy to try to keep me
from doing the “Dumbshit Driver” routine.. (driving with the turn signals on)
But the
sound was still feeble compared to the exhaust note.. So ror76-1.jpg and ror76-2.jpg show the good fix. A bright clearance light on the dash
wired across the flasher..
That should get my attention.
When I
first put it on I had the mount grounded and the hot lead to the load side of
the flasher. That did not work
since the current through the heater element in the flasher caused the lamp to
be on dimly when ever the ignition was on. Then it would flash bright when the signals were on. So I insulated the ground plate
and ran two wires to put the lamp in parallel with the flasher. When the turn signal bulbs are lit the
dash indicator is off and vice versa..
Another
little project was the choke. I
have been fooling with the choke pushrod adjustment to get Goody to start and
idle in the cool damp and yet release the secondaries when it came time to
boogie.. I could not
do it..
So,
ror76-3.jpg shows the final solution.
I was
going to install it today but I had another trip to town.. (in Rustpuppy, fun!)
So it
goes in tomorrow.. The
odd shaped hole between the mysterious little black electronic box and the
instruments is where the choke knob will live..
More to
come..
Rick
Draganowski
(manual
chokes is good)
p.s. 177 more miles and the “mysterious
little black electronic box” will start being turned on..
Subject: Totally disgusting mouse story
Date: Sunday,
October 22, 2000 6:13 PM
I spent
a little time today getting the Lakewood Competition traction bars installed on
Rustpuppy.
That is not
the subject of this report.
Anyway,
the first step was popping the Moon wheel cover off of Rustpuppy’s right rear
wheel.
I
noticed a lot of fine gray fur on the inside edges of the Moon when I was
prying it off. When it finally
popped free I was subjected to the sight of a, dead, dried out, and in very
poor condition, mouse.. (mouse.jpg)
The damn
thing was starting to make a nest in the Moon, getting in through the holes in
the Rallye wheel.. (thanks Rob
Roberson)
The
centrifugal forces involved in riding the wheel did a lot of damage to the
mouse. It’s internal organs were
still stuck on the wheel.
(mouse1.jpg)
Gross
out time.. I just hope this
is the little bastard that pooped all over Goody..
More to
come..
Rick
Draganowski
(got 90%
finished installing the right bar..)
Subject: Return of Rustpuppy report 77
Date: Monday,
October 23, 2000 9:51 PM
The
attack on the 24 year old nuts and bolts to get the Lakewood Competition
traction bars on started Sunday and didn’t get to a reportable stage till this
evening.. You already know
about the nasty mousie story so this episode starts with a teeny safety
lesson.. Lotsa torque has to
be used to get those 11/16 nuts off of the U-bolts and T-bolts so I made sure
that a jackstand was under the tail..
( ror77-1.jpg, note the little bit of rust in the quarter panel)
The old
shock was off in a jiffy.. Come to
find out that this shock has been the source of the banging rattle in the rear of
Rustpuppy since I got her in ‘94.
With the new shocks on during seat time that annoying rattle was
gone.. Cool.. (ror77-2.jpg) The shock at full travel is the limit on the axle
movement going down.. I had heard
that this was bad but later on I found a good reason for it..
This
next shot shows the mounting holes for the top of the shock.. Alex Bilan would be happy to know that
there is very little rust under Rustpuppy.. She has never been in a place which salts the
roads so the rust is just cosmetic..
(ror77-3.jpg... A most
endearing feature.. Mechanically
sound but looking like total junk)
More
safety lectures.. Every time I
have the wheels off of Rustpuppy I check the brakes. This is important. Looking good back here.. (ror77-4.jpg, ror77-5.jpg)
You can
see the stealthy powder coated bar in ror77-6.jpg. Really heavy and top quality..
This next
picture shows the down side of removing the shock and letting the axle drop a
couple more inches.. The stock
brake line is too short and it put a hell of a strain on it.. It even bent the bracket which attaches
the T-fitting to the axle.
(ror77-7.jpg) This pic was
taken today after dark with the drop light.. I got a late start and really wanted to finish up so I
was out working in the dark, on an old car, with the drop light.. It made me feel like a kid again..
You can
see that with the shock on the strain is taken off the brake hose..
(ror77-8.jpg)
Here is
the mostly finished result. The
bars angle down at about 2.75 degrees.. (ror77-9.jpg) And the rubber bumpers need to go on..
I wish I
knew for sure what I was doing..
More to
come..
Rick
Draganowski
(less
than 100 miles to go to get to the magic 500 on Goody..)
Subject: Return of Rustpuppy report 78
Date: Wednesday,
October 25, 2000 9:14 PM
The
Lakewood Competition traction bars are completely in. Poor Rustpuppy has a serious case of sagging springs in the
rear. The result is the bars are
too close to the springs. (and to the ground) I cut the rubber bumpers down to 1 inch tall each and on a
level road they just touch the spring eyes on both sides. The spring rate has increased due to
the front half of the springs being out of service and Rustpuppy is riding hard
in the back. (see ror78-2,jpg) (it is sort of like John Soliday’s S&M bars
do to his Nova)
Note the
marks left on the bottom front of the bar from encountering the ground.. (have learned to be more careful
but still drag them once in a while.. beat up old country road..)
But
there is a bright side to the story..
The tightening up of the rear suspension has made the high speed
tracking of Rustpuppy considerably improved.. (not comfortable but safer..)
And the
acid test.. (launches)
Yippee! They really work.. It is weird to feel the rear end of
Rustpuppy go up with the front on acceleration but the traction is greatly
improved.. Probably more than 4
times better than before..
This is
good for the numbers which will show up when the G-Tech starts lighting up them
red numbers on the dash..
Just 66
miles to go to get to the magic 500 mark.
Then another oil and filter change and it is time to rock and roll..
In the
interior I pulled off the teeny electric defogger mounted on the dash and
installed a much larger one (also from JCWhitney) directly into the defroster
duct so the stock ducts can be used..
Complete with a nice switch on the dash.. Now I have to redo the top dash treatment.. Probably going to fold some aluminum
flashing, paint if flat black and cover the whole dash with holes for the
choke, G-Tech, and defogger switch.. But not too soon..
Also I
have decided that due to the cam change the stock choke stove just cannot be
set completely properly.. The
problem is when Goody is not either cold (from sitting for several hours) or
hot (just ran a while) but when she is in the middle (ran mebbe an hour
ago). The choke does not come on
enough to engage the fast idle cam so she wants to die for the first few
minutes.. Annoying..
So I am
going to go ahead and put in the manual choke I flanged up last week..
More to
come..
Rick
Draganowski
(66 miles
and an oil change..)
Subject: Return
of Rustpuppy report 79
Date: Monday,
October 30, 2000 8:18 PM
Just a
tad of Rustpuppy work since last report.
I have been troubled by the positive camber problem on the left front
wheel and worked up a measurement technique for it.. My flangeup sez that I need to add 0.150 of
shims to get the wheel at 0 degrees camber.. The right front is at zero already.. I plundered Yakima Sue for some shims
and put in 0.125.. The
thinnest ones I got are 0.0625 but I need about another 0.025.. I measured it again today but
have not done the calculations yet.. Anyway it is still cambered positive about 1/8” at the
edge of the wheel..
Rustpuppy
got the 500 miles on Goody this weekend.
But the nastiest coldest wettest damn storm started Saturday morning and
didn’t clear up till late last night.
We had
sunshine today though and I really wanted to change the oil.. But with my bumper jack
non-compos-mentis it is a difficult job to get the front end up high enough to
wedge my fat ol’ bod under there..
So..
I went
out this evening to Rustpuppy Run anyway..
It was
calm and still. Just after dark
but before the condensation screws up the traction..
The
first run (Southbound) went really well.
Good launch with about 1 revolution of tire spin and go..
I let
the TH350 shift.. (the damn
thing is shifting at 4500rpm with the Ford juice in it.)
Rustpuppy
ran 14.42@100.2
on the G-Tech..
On the
Northbound run the condensation had already started and I picked up enough
wheelspin to cause featherfooting.
But Rustpuppy turned 14.62@99.7
anyway.
This is
shifting at 4500rpm. Wait
till we start shifting at 6000....
More to
come..
Rick
Draganowski
(more
than half way into the 14’s while shifting at 4500.. Happy happy, joy joy..)
Subject: Return of Rustpuppy report 80
Date: Tuesday,
October 31, 2000 7:47 PM
I have felt
a little funny about the poor appearance being presented to my neighbor of
Yakima Sue up at the top of my lawn.
So over the last couple of days I tried to improve them. I managed to get the beautiful and
perfect right front fender out of the passengers compartment and put it in
place held with some bungees to keep it from carrying away in the expected
winter storms. While wrestling out the Disco bumper which was protruding from
the missing front window Yakima bit me a good one. Crushed my thumb..
Ow.. She does not fancy
being a parts car for Rustpuppy and the Dawg I guess.. Then again I got attacked while tucking
the bumper out of sight in the engine compartment. Anyway, from a distance she looks almost presentable.
I also
battened down the hatches on Junkyard Dawg to be sure that the loose windshield
cannot blow off in the next storm and get broken.
On the
important news front I took Rustpuppy out for some seat time today.
I wanted
to practice slamming shifts with the Pro-matic ratchet shifter. It is a bummer but it cannot be done in
a sane civilized way as the stupid TH350 upshifts to second at partial throttle
automatically. It stays in
first at full throttle though.
It was a
little (actually a lot) disconcerting on the 1-2 shift at full throttle 5700rpm
as the rear wheels break loose and there is a nasty slide to the right by the
rear end.. You have to be on top
of it..
I got
one 0-60 time during practice of 5.43 seconds..
All
pumped up on adrenalin and with a flock of butterflies in my fat ol’ stomach I
took Rustpuppy out on the Rustpuppy Run just at dusk. There is another damn cold front coming in so the
temperature was dropping and the condensation coming down early but what the
hell.. I was cooking with
gas.. (and a bit of empty headed
emotion..)
The
first run (Southbound) had a poor launch due to enough wheelspin caused by the
damn dew to force me to get almost completely off the gas whereupon the stupid
tranny upshifted to second gear and then downshifted to first when I got back
on the gas.. (must have lost some
time there)
Anyway
the run went very well after the stupid launch problems and Rustpuppy came up
with 14.33@103.6 Too cool..
I was
shifting at 5700 instead of the tranny autoshifting at 4500..
I drove
down to the turnaround rest stop with more calmness than I expected. I had been pretty worried about the
nasty kick to the right on the 1-2 shift as Rustpuppy Run is a bit narrow for
hi-jinks..
The
Northbound run was better. I just
rolled on the gas easy to compensate for the dew on the track and got a nice
(but slow) launch. The sound
of Goody at 5700 was more of a guide to shifting than the tach as it is
essential to keep your eyes on the road on Rustpuppy Run.. (remember the 20 foot drop to the
floodplain) I gotta get a
tach with a shift light now..
Hmmm.. It is always
something..
The time
was 14.25@103.6 And that without a hard
launch.. Rustpuppy is smiling..
Note that
the mph numbers stayed the same..
Goody is running good..
More to
come..
Rick
Draganowski
(still have
a few butterflies..)
Subject: Black Friday
Date: Saturday,
November 04, 2000 7:22 PM
I
started the day with finding out about Ray’s heart attack.. That was the big news and it put me
into a very dark mood as I drove to town to take care of business. (Ray will be OK but I didn’t know
it at the time)
Then I
noticed an unusual amount of noise from Rustpuppy’s rear end as I went down the
hill to get to the highway. There
was always a tiny bit of whine when on the overrun with the backside of the
ring gear being used but it seemed really loud.
Then
when I got on the highway it was whining on acceleration and cruise. It had never done that before. With a sinking feeling in my heart I
thought about turning back but I rationalized it away enough to complete the 15
mile trip to town. Slowing down
for the 30mph limit in town with the differential up to operating temp with the
lube thin the howling was very pronounced..
it seems
like the engagement between the ring and pinion gears has shifted. Usually one or more of the pinion
bearings cause this from my limited experience..
Anyway
there will be no more Rustpuppy runs till this issue is resolved.
Damn.
At least
Ray is going to be OK (but keep praying as he is still overworks too much)
I jacked
Rustpuppy up and put jackstands under the rear to allow running with the wheels
off the ground. Then I made two
recordings of the whine with the new 10 buck microphone and the Sony Vile.
The
first mp3 is the sound of it coasting down in neutral from about 50mph with the
motor off.
The one in the addendum is the sound from accelerating the wheels and the nasty little bearing rattle at idle.
Damn again..
Rick
Draganowski
(what will I
do?)
Subject: Black Friday addendum 1
Date: Saturday,
November 04, 2000 7:25 PM
(whine4c.mp3)
Rats..
Yakima
Sue has a 2.73 ratio 7.5” rear end which may be ok..
Poop..
Rick
Draganowski
(need a
complete rear end 8.5” 3.08 or better..
or even a good 7.5” 3.08..
sigh..)
Subject: Return of Rustpuppy report 82
Date: Sunday,
November 12, 2000 6:31 PM
As the
list knows from the Black Friday message I seem to have toasted the 7.5” rear
axle in Rustpuppy. The weather has
turned against me bigtime (winter sucks) so not much progress. I got Rustpuppy up on the jackstands in
preparation for dropping out the axle.
(ror82-1.jpg)
I took a
snapshot of the excellent 8.5” axle under the Suburban.(has a Detroit Locker in
it too) It sure looks nice and hefty.. (ror82-2.jpg) Looking up Rustpuppy’s
hinder shows the spindly little 7.5” job..
Ror82-4.jpg
shows the limited clearance I am going to be working in.. I am thinking of pulling the gas tank
and replacing the sock and cleaning it up as well as getting new hoses on it.
Today I
popped the rear wheels and brake drums (trying to get even a tiny bit done each
day). I got the idea of running
Rustpuppy with the wheels off so I could use the ol’ screwdriver handle to the
ear noise monitoring trick..
The damn axle made no noise at all! Starting to think strange thoughts I put the wheels
back on. The howling came back
pronto.. Evidently without any
kind of load the grease muffles the sounds so it sounds good.. So then the wheels came back off.. An exercise in futility..
I got my
ducks in a row on convincing my mechanic that the cheaper 2 series posi carrier
with a spacer would be just fine for Rustpuppy (and save some bucks) I am hoping to get a rebuilt 8.5” axle
with the posi and 3.42 gears soon.
I really need to get back on the road with ol’ Rustpuppy..
It is always
something..
More to
come..
Rick
Draganowski
(thought
for a few minutes it had healed up..
no such luck)
End of
Chapter 9